NHTSA Complaint #10247092 — 2003 DODGE RAM 3500
FUEL SYSTEM, DIESEL issue reported to NHTSA
Complaint Details
| ODI Number | 10247092 |
| Vehicle | 2003 DODGE RAM 3500 |
| Component | FUEL SYSTEM, DIESEL |
| Date of Incident | |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | LA |
Consumer Description
STARTED NOTICING TRUCK HARD TO START, THEN IT DIES AT IDLE, IN TRAFFIC ETC, IT HAPPENS ABOUT ANYWHERE FROM 4 TIMES A DAY TO 4 TIMES A WEEK JUST DEPENDS, TOLD THAT THE TRUCK TRANSFER PUMP IS A DEALER ITEM ONLY AT ABOUT 400.00 OVER THE COAST OF INTERNET PRICING FOR THE KIT, WOULDN'T THIS BE A RECALL? I HAVE SEARCHED AN FOUND NUMEROUS OTHER COMPLAINS ON THIS SAME PROBLEM , BUT SINCE DODGE DISCONTINUED THE EXTERIOR TRANSFER PUMP THEN IT WAS A DESIGN FLAW AND SHOULD BE A RECALL I HAD MY TRUCK DIE ON MY 2 TIMES TODAY IN TRAFFIC MOVING 70 MILES AN HOUR WITH KIDS IN THE BACK SEAT AND AN 18 WHEELER BEHIND ME , THE TRUCK HAS NO OTHER PROBLEMS BUT I DON'T THINK DODGE SHOULD BE ALLOWED TO CHANGE THE DESIGN WITH OUT HAVING A RECALL. *TR
Related Complaints for the 2003 DODGE RAM 3500
Other FUEL SYSTEM, DIESEL Complaints
#10393906
SEEMS TO OCCUR WHEN IT IS DAMP OR RAINING. DOESN'T OCCUR WHEN IT IS DRY. REVS UP ON ITS OWN, EVEN IN GEAR WITH FOOT O...
#10357192
THE LIFT/TRANSFER PUMP OF THE FUEL SYSTEM FAILED WHILE DRIVING ON THE FREEWAY. (SEPARATE FROM THE MAIN FUEL PUMP ). ...
#10335728
FAILURE OF 2003 DODGE RAM 3500 WITH HO DIESEL ENGINE AND MANUAL 6 SPEED TRANSMISSION - ENGINE TURNS OVER BUT FAILS TO...
#10158363
WHEN TOWING WITH THE VEHICLE IT DOES NOT RESPOND WHEN PRESSING THE GAS PEDAL. HAVE TO PULLOVER LET TRUCK REST FOR A...
Recent Complaints for the 2003 DODGE RAM 3500
#11604425
SUSPENSION
The contact owns a 2003 Dodge Ram 3500. The contact stated while driving at various speeds, there was a clunking soun...
#11331110
STRUCTURE:BODY
FRAME RUSTED THROUGH IN SEVERAL PLACES. SERVICE PROVIDER HAD PROBLEMS PLACING TRUCK ON LIFT DUE TO FRAME INTEGRITY TO...
#11151794
POWER TRAIN
HAD TO REPLACE CARRING BEARING AND SLEEVE BUSHING ON DRIVE SHAFT HAD A LOT OF WABLE IN STEERING