NHTSA Complaint #10658584 — 2011 MINI COOPER S COUNTRYMAN
POWER TRAIN issue reported to NHTSA
Complaint Details
| ODI Number | 10658584 |
| Vehicle | 2011 MINI COOPER S COUNTRYMAN |
| Component | POWER TRAIN |
| Date of Incident | |
| Date Filed | |
| Mileage | 27,542 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | IA |
Consumer Description
ON OCTOBER 7TH, 2014 THE KEY WOULD NOT COME OUT OF THE KEY SLOT. THE KEY IS NOT REQUIRED TO BE INSERTED TO START THE CAR BUT SIMPLY WITH YOU. HOWEVER, MY DAUGHTER HAD BORROWED THE CAR AND INSERTED THE KEY SO I HAVE NO WAY OF KNOWING IF THIS FAILURE OCCURRED ON THE DATE MENTIONED OR EARLIER. IT WAS IN FOR SERVICE ON AUGUST 25TH, 2014 SO SOMETIME BETWEEN THE TWO DATES THE FAILURE OCCURRED. I TOOK IT TO OUR LOCAL DEALER, MINI OF DES MOINES, AND THEY ALSO COULD NOT REMOVE THE KEY. THEY NOTICED THAT WITHOUT THE CAR RUNNING AND THE BRAKE PEDAL NOT DEPRESSED THE AUTOMATIC TRANSMISSION SHIFTER COULD BE MOVED TO ANY POSITION. THEY DID NOT KNOW IF THIS WOULD OCCUR WITH THE CAR RUNNING, I.E. INADVERTENTLY HITTING THE SHIFTER INTO REVERSE OR PARK WHILE DRIVING. THEY ALSO DID NOT KNOW IF THE CAR WAS ACTUALLY IN PARK WHEN INDICATED SO. I LEFT THE CAR, WAS GIVEN A LOANER, AND WHEN THEY CALLED ME THE DIAGNOSIS WAS THAT LIQUID HAD SPILLED IN A CUP HOLDER AND LEAKED THROUGH THE UNSEALED SCREW IN THE BOTTOM ONTO AN ELECTRICAL COMPONENT CAUSING THE PROBLEM. I AM WELL AWARE OF LIQUID SPILLING INTO THE CUP HOLDER AS THIS HAPPENED A COUPLE OF TIMES WHEN I FIRST GOT THE CAR DUE TO THE SPRING LOADED HOLDERS IN THE SIDE OF THE CUP HOLDER THAT I THEN REMOVED . THEY ARE ENGINEERED INCORRECTLY AND ALTHOUGH THE MANUAL STATES TO USE "LIGHTWEIGHT, NON-BREAKABLE CONTAINERS" THESE SPRING RETAINERS WILL POKE A HOLE IN STYROFOAM CUPS AND WILL COMPRESS A PAPER CUP, LIKE STARBUCKS, ENOUGH THAT LIQUID WILL EXPEL THROUGH THE TOP VENT HOLE AND DRINKING SLOT. IN ADDITION, WHILE ONE WOULD ASSUME THAT LIQUID WOULD OCCASIONALLY BE SPILLED IN A CUP HOLDER, AN ADDITIONAL ENGINEERING ERROR WAS MADE WHEN NO SEALING WASHER WAS USED ON THE RETAINING SCREW IN THE BOTTOM AND ANY LIQUID THE WOULD LEAK ON TO ANOTHER UNSEALED COMPONENT AND CAUSE THIS FAILURE. A $1,100.00 REPAIR COST FOR BMW'S INEPT ENGINEERING???
Related Complaints for the 2011 MINI COOPER S COUNTRYMAN
Other POWER TRAIN Complaints
#10538114
WITH JUST OVER 16000 MILES ON MY 2011 MINI COOPER S COUNTRYMAN, MY CLUTCH IS BURNED OUT! HAVING IT TOWED TO THE CLOSE...
#10508465
VEHICLE STALLS FROM 1ST GEAR WITHOUT THE ASSISTANCE OF THE "SPORT" BUTTON (REGARDLESS OF TERRAIN). COMPONENTS IN THE...
#10477412
AT 18XXX MILES THE CLUTCH IS GONE. TRANSFER CASE FOUND DEFECTIVE. THE CLUTCH HAS BEEN FAILING ON THE ALL4 MODELS AL...
#10462518
2011 MINI COUNTRYMAN S ALL4 MANUAL TRANSMISSION AFTER REPEATED INCIDENTS OF THE CLUTCH "SMOKING" UNDER HEAVY USE, AN...
Recent Complaints for the 2011 MINI COOPER S COUNTRYMAN
#11644516
ELECTRICAL SYSTEM
My father has the same year mini cooper and has a recall on the foot control module. He actually just got it fixed e...
#11644516
ENGINE
My father has the same year mini cooper and has a recall on the foot control module. He actually just got it fixed e...
#11644516
EXTERIOR LIGHTING
My father has the same year mini cooper and has a recall on the foot control module. He actually just got it fixed e...
#11587828
ELECTRICAL SYSTEM:12V/24V/48V BATTERY
The contact owns a 2011 Mini Cooper S Countryman. The contact stated that while the vehicle was parked, the battery b...
#11587828
EXTERIOR LIGHTING:BRAKE LIGHTS
The contact owns a 2011 Mini Cooper S Countryman. The contact stated that while the vehicle was parked, the battery b...