NHTSA Complaint #10491124 — 2007 FORD F-150
ENGINE AND ENGINE COOLING issue reported to NHTSA
Complaint Details
| ODI Number | 10491124 |
| Vehicle | 2007 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | TN |
Consumer Description
WAS EXPERIENCING A SHUTTER SIMILAR TO THE FEELING OF A MISFIRE WHEN ACCELERATING UP A GRADE FROM LEVEL ROAD CONDITIONS. THIS SHUTTER WAS BETWEEN 1250 AND 1500 RPM. TOOK THE VEHICLE TO FORD DEALERSHIP WHO ELIMINATED COIL PACK AND TORQUE CONVERTER AS THE SOURCE OF THE PROBLEM. I HAD TAKEN ANOTHER VEHICLE I OWN TO A REPAIR SHOP I HAVE USED FOE SEVERAL YEARS FOR AN OIL CHANGE AND WHEN I PICKED UP MY VEHICLE I MENTIONED THE PROBLEM I WAS HAVING WITH MY 2007 FORD F150 AND THEY ADVISED THAT MY PROBLEM WAS PROBABLY MISFIRE ON ONE OR MORE PLUGS. THEY ADVISED ME THAT THEY HAD DEALT WITH THIS SAME PROBLEM OVER THE PAST FEW YEARS. THEY PROCEEDED TO INFORM ME THAT THERE WAS A MAJOR PROBLEM WITH REPLACING THE PLUGS-THEY COULD BREAK WHEN REMOVING. IF THAT HAPPENS AND IT DID (4 PLUGS BROKE) THEN ADDITIONAL LABOR COSTS WOULD BE ADDED TO MY BILL. END RESULT A BILL FOR $600.00 TO REPLACE 8 SPARK PLUGS. ABSOLUTELY ABSURD. AS A PART OF THIS EXPERIENCE I HAVE LEARNED THAT FORD MFG THIS ENGINE FROM 2005-2007 AND WHEN THIS ISSUE BEGAN TO SURFACE THAT THEY CHANGED THE ENGINE DESIGN TO ELIMINATE THIS PROBLEM. FORD WAS OBVIOUSLY AWARE THAT A FUTURE PROBLEM WAS GOING TO BE FACED BY THE CONSUMER. WHY SHOULD WE THE CONSUMER HAVE TO BEAR THE FULL EXPENSE TO PAY FOR THEIR FLAWED DESIGN IN THIS ENGINE. THEY SHOULD BE WILLING TO ADMIT THEIR MISTAKE BUT APPARENTLY IT IS GOING TO TAKE SOME LEGAL PRESSURE TO GET THIS DONE. IF THEY DO NOT STEP UP I WILL NEVER BY ANOTHER FORD.
Related Complaints for the 2007 FORD F-150
Other ENGINE AND ENGINE COOLING Complaints
#10706090
WENT TO HAVE TRUCK TUNED UP--MECHANIC WOULD NOT EVEN TOUCH SPARK PLUGS BECAUSE THEY BREAK OFF AND THE ENTIRE HEAD HAS...
#10639604
NOTICED LEAKAGE UNDER FRONT LEFT TIRE. ALL TRANSMISSION FLUID HAD LEAKED OUT. TRANSMISSION OIL LINE RUSTED THROUGH....
#10627873
I WAS DRIVING DOWN THE HIGHWAY AND AS I WAS MAKING A RIGHT HAND TURN MY MOTOR TURNED OFF. I HAD NO STEERING AND LITTL...
#10484512
TL* THE CONTACT OWNS A 2007 FORD F-150. THE CONTACT STATED THAT WHILE DRIVING 55 MPH WITH THE CRUISE CONTROL ACTIVAT...
#10451974
2007 F 150 KING RANCH SPARK PLUGS BREAK WHEN REMOVING THEM (FORD CHEAP SPARK PLUG SYSTEM). THE TRUCK ALSO PULL/TUGS L...
Recent Complaints for the 2007 FORD F-150
#11686991
STEERING
After making a sharp right turn tie rod came loose from steering rod. After inspection the threads on the steering r...
#11661836
POWER TRAIN
The contact owned a 2007 Ford F-150. The contact stated that when depressing the accelerator pedal while in reverse, ...
#11630143
POWER TRAIN:AUTOMATIC TRANSMISSION:TORQUE CONVERTER
The contact owns a 2007 Ford F-150 The contact stated while driving at an undisclosed speed, the vehicle stalled and ...
#11627107
POWER TRAIN
Transmission and rear end jerking when putting in or taking out of park, reverse or drive and now doesn't want to go ...
#11627107
STEERING
Transmission and rear end jerking when putting in or taking out of park, reverse or drive and now doesn't want to go ...