NHTSA Complaint #10275771 — 2002 FORD F-150
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10275771 |
| Vehicle | 2002 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 55,082 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | TX |
Consumer Description
MY 2002 FORD F150 TRUCK, WITH THE 5.4 LITER ENGINE, HAS HAD 2 FAILURES ON 2 DIFFERENT OCCASIONS IN THE SPACE OF 8 MONTHS. EACH TIME I WAS JUST DRIVING DOWN THE HIGHWAY AND A SPARK PLUG WAS BLOWN OUT OF THE HEAD, ALONG WITH THE COIL. (PLUG #3 THE FIRST TIME AND #7 THE LAST TIME.) THIS FAILURE CAUSED AN IMMEDIATE LOSS OF POWER. LUCKILY THE TRAFFIC WAS LIGHT EACH TIME, BEING LATE AT NIGHT, SO I WAS ABLE TO PULL SAFELY TO THE SIDE OF THE ROAD TO DETERMINE THE PROBLEM, WHEREAS IF THE TRAFFIC HAD BEEN HEAVY, IT COULD HAVE CAUSED A MAJOR ACCIDENT BECAUSE OF THE IMMEDIATE POWER LOSS TO THE ENGINE, AND/OR A FIRE DUE TO IT PROXIMITY TO THE INJECTORS. THE DEFECTS WERE REPAIRED AT THE LOCAL FORD DEALERSHIP WHERE THE TRUCK WAS PURCHASED USING A THREADED INSERT INTO THE OLD HEAD AND A NEW COIL. TOTAL COST FOR BOTH REPAIRS WAS APPROXIMATELY $600, AT MY EXPENSE. I HAVE EMAILED FORD MOTOR COMPANY AND THEY RESPONDED SAYING THAT BECAUSE THE VEHICLE WAS OUT OF WARRANTY AND THERE WERE NO RECALLS OR CUSTOMER SATISFACTION PROGRAMS IT WOULD NOT BE FIXED BY FORD. I PURCHASED THIS VEHICLE NEW AND IT HAS BEEN METICULOUSLY MAINTAINED. I HAVE SEARCHED THE INTERNET AND HAVE FOUND THAT THERE ARE THOUSANDS OF THESE ENGINES WITH THIS PROBLEM. IT IS OBVIOUS FORD KNOWS OF THIS DEFECT IN THE HEADS AND REFUSES TO DEAL WITH IT. IF NOT BY RECALL, IT IS OBVIOUSLY A FACTORY DEFECT AND SHOULD BE DEALT WITH BY FORD AS THE INCIDENTS OCCUR. THIS IS A DANGEROUS SITUATION THAT SHOULD BE LOOKED INTO BECAUSE OF THE IMMEDIATE LOSS OF ENGINE POWER AND POSSIBILITY OF FIRE. *TR
Related Complaints for the 2002 FORD F-150
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10417002
TURNED OVER MY 2002 FORD F-150. A LOUD POP OCCURRED AS A SPARK PLUG/COIL PACK BLEW OUT. THIS IS THE 3RD COIL PACK THA...
#10416778
WENT TO MAKE AN APPOINTMENT WITH FIRESTONE TO HAVE MY PLUGS CHANGED PER FORD MANUAL ON MY 2002 F150 5.4 LITER V8. IT ...
#10407195
I WAS DRIVING HOME FROM WORK DOING ABOUT 35MPH AND A LARGE AND LOUD POP FOLLOWED BY REPEATED QUIETER POPPING SOUND UN...
#10404119
2002 FORD F-150 WITH A 5.4L TRITON V8. THE #7 SPARK PLUG BLEW OUT OF THE PORT AND BROKE THE COIL. THAT LEFT FUEL VAPO...
#10392188
I HAVE A FORD F-150 THAT HAS A TRITON V-8 MOTOR. IT HAS 110,000 MILES. I HAVE HAD THE TRUCK FOR 3 YEARS AND PURCHASED...
Recent Complaints for the 2002 FORD F-150
#11661168
SEAT BELTS
Front seatbelts on 2002 Ford F-150 become unlatched unexpectedly while driving. This has been noticed over the last t...
#11604628
FUEL/PROPULSION SYSTEM
DRIVING DOWN [XXX] THE STRAPS ON MY GAS TANK BROKE BECAUSE THEY RUSTED THRU CAUSING GAS TANK TO DROP AND SPILL FUEL A...
#11604628
UNKNOWN OR OTHER
DRIVING DOWN [XXX] THE STRAPS ON MY GAS TANK BROKE BECAUSE THEY RUSTED THRU CAUSING GAS TANK TO DROP AND SPILL FUEL A...
#11591276
ENGINE
The contact owns a 2002 Ford F-150. The contact stated while driving at an undisclosed speed, the vehicle made a loud...