NHTSA Complaint #10136115 — 2002 FORD F-150
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10136115 |
| Vehicle | 2002 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 60,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | CA |
Consumer Description
SPARK PLUGS BLOWN OUT OF CYLINDER HEAD WHILE DRIVING THROUGH THE DESERT. THE FRONT AND REAR SPARK PLUG ON THE DRIVER'S SIDE OF THE ENGINE BLEW OUT WITHIN A 24 HOUR PERIOD. I WAS DIVING TO OREGON EARLY FRIDAY MORNING WHEN THE REAR SPARK PLUG ON THE DRIVERS SIDE OF THE ENGINE BLEW OUT. I WAS STUCK IN THE DESERT FOR 9 HOURS. CALLED AAA AND WAS TOWED BACK TO WINNEMUCCA ON FRIDAY NIGHT BEFORE LABOR DAY WEEKEND. NO REPAIR FACILITIES AVAILABLE BUT THE TOW YARD GUY HAD SOME JB WELD. I PUT SOME ON THE THREADS OF THE SPARK PLUG AND SCREWED IT BACK INTO WHAT LITTLE THREADS REMAINED IN THE CYLINDER HEAD. I WAS SUPPOSED TO BE AT WORK THE FOLLOWING SATURDAY MORNING. I LET THE JB WELD SET FOR 5 HOURS. WHEN I LEFT WINNEMUCCA IT WAS 1:30 AM SATURDAY. I DROVE FROM WINNEMUCCA NEVADA TO AUBURN CALIFORNIA , NEARLY 270 MILES WHEN I BLEW ANOTHER SPARK PLUG THIS TIME THE FRONT ONE ON THE DRIVERS SIDE. THEN I HAD TO BE TOWED TO SAN JOSE CALIFORNIA. OBVIOUSLY I MISSED WORK THAT SATURDAY, BUT MY BOSS WAS KIND ENOUGH TO RESCHEDULE THE WORK FOR SUNDAY. THE FACT THAT THE SPARK PLUG THAT HAD NOT BEEN REPAIRED (THE FRONT PLUG) BLEW OUT WHILE THE REPAIRED ONE DID NOT BLOW OUT TELLS ME THAT ALL OF MY SPARK PLUGS ARE PROBABLY HANGING ON BY A THREAD. IF I DID NOT HAVE A CELLULAR PHONE WITH SERVICE WHEN THE FIRST PLUG BLEW OUT, I DON'T THINK I WOULD HAVE MADE IT OUT OF THAT DESERT 70 MILES NORTH OF WINNEMUCCA ON I-80. THERE IS NOTHING OUT THERE. NOTHING. NO PHONE, NO WATER, NO PEOPLE, EXCEPT FOR THE BIG TRUCKS THAT BLOW BY EVERY ONCE IN A WHILE AT 90 MPH WHILE YOUR TRYING TO FIX YOUR P-O-S BROKEN DOWN 2002 FORD F-150 LIGHTNING ON THE SIDE OF A 2 LANE HIGHWAY. *NM
Related Complaints for the 2002 FORD F-150
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10417002
TURNED OVER MY 2002 FORD F-150. A LOUD POP OCCURRED AS A SPARK PLUG/COIL PACK BLEW OUT. THIS IS THE 3RD COIL PACK THA...
#10416778
WENT TO MAKE AN APPOINTMENT WITH FIRESTONE TO HAVE MY PLUGS CHANGED PER FORD MANUAL ON MY 2002 F150 5.4 LITER V8. IT ...
#10407195
I WAS DRIVING HOME FROM WORK DOING ABOUT 35MPH AND A LARGE AND LOUD POP FOLLOWED BY REPEATED QUIETER POPPING SOUND UN...
#10404119
2002 FORD F-150 WITH A 5.4L TRITON V8. THE #7 SPARK PLUG BLEW OUT OF THE PORT AND BROKE THE COIL. THAT LEFT FUEL VAPO...
#10392188
I HAVE A FORD F-150 THAT HAS A TRITON V-8 MOTOR. IT HAS 110,000 MILES. I HAVE HAD THE TRUCK FOR 3 YEARS AND PURCHASED...
Recent Complaints for the 2002 FORD F-150
#11661168
SEAT BELTS
Front seatbelts on 2002 Ford F-150 become unlatched unexpectedly while driving. This has been noticed over the last t...
#11604628
FUEL/PROPULSION SYSTEM
DRIVING DOWN [XXX] THE STRAPS ON MY GAS TANK BROKE BECAUSE THEY RUSTED THRU CAUSING GAS TANK TO DROP AND SPILL FUEL A...
#11604628
UNKNOWN OR OTHER
DRIVING DOWN [XXX] THE STRAPS ON MY GAS TANK BROKE BECAUSE THEY RUSTED THRU CAUSING GAS TANK TO DROP AND SPILL FUEL A...
#11591276
ENGINE
The contact owns a 2002 Ford F-150. The contact stated while driving at an undisclosed speed, the vehicle made a loud...