NHTSA Complaint #10125621 — 1990 FORD F350
FUEL SYSTEM, GASOLINE:STORAGE:AUXILLARY TANK:SELECTOR DEVICES issue reported to NHTSA
Complaint Details
| ODI Number | 10125621 |
| Vehicle | 1990 FORD F350 |
| Component | FUEL SYSTEM, GASOLINE:STORAGE:AUXILLARY TANK:SELECTOR DEVICES |
| Date of Incident | |
| Date Filed | |
| Mileage | 44,470 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | CA |
Consumer Description
DT: THE CROSS OVER OF THE FUEL IMPROPERLY OVERFILLS THE SECOND TANK, SPILLING FUEL OUT OF VEHICLE. THERE WERE 2 SAFETY RECALLS OF THIS ITEM. BUT FORD WAS SAYING THAT ONE RECALL WAS TAKEN CARE OF BY A PREVIOUS OWNER. THE SECOND RECALL EXPIRED, AND FORD WILL NOT FIX THIS PROBLEM. FORD HAS BEEN CONTACTED BY THE CUSTOMER AND THE REPAIR FACILITY. FORD WAS STILL NOT WILLING TO HELP. THIS HAS BEEN A PROBLEM FOR A COUPLE OF MONTHS. THE CUSTOMER WAS HAVING IT REPAIRED AT HIS OWN EXPENSE. IF THERE WAS A SAFETY ISSUE ON THIS PROBLEM IT SHOULD BE TAKEN CARE OFF BY DEALER NO MATTER HOW MANY TIMES IT COMES UP.*AK *JB
Related Complaints for the 1990 FORD F350
Other FUEL SYSTEM, GASOLINE:STORAGE:AUXILLARY TANK:SELECTOR DEVICES Complaints
Recent Complaints for the 1990 FORD F350
#10089939
FUEL SYSTEM, GASOLINE:STORAGE:AUXILLARY TANK
VEHICLE WAS TAKEN TO DEALER FOR RECALL REPAIRS ABOUT 5 YEARS AGO. VEHICLE HAD DUEL GAS TANKS. THE RECALL WAS ISSUED...
#10024386
TIRES:TREAD/BELT
WHILE TRAVELING, THE CONSUMER HEARD A LOUD POPPING NOISE. THE CONSUMER PULLED OVER AND SAW THE RIGHT FRONT TIRE TRE...
#757905
FUEL SYSTEM, GASOLINE:DELIVERY
I AM SPEAKING ON BEHALF OF THE OWNER, I AM TED SCHORE OF OCALA,FL PINEYWOODS AUTOMOTIVE 352-629-6727 THE CUSTOMER HAD...
#757633
FUEL SYSTEM, GASOLINE:STORAGE:TANK ASSEMBLY
THERE HAS BEEN MULTIPLE RECALL NOTICES FOR THE FORD F-SERIES DUAL FUEL TANK DESIGN FLAW. WHEN BOTH TANKS ON MY TRUCK ...
#897741
ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE
WHILE DRIVING EMERGENCY SPARE TIRE UNDERNEATH VEHICLE CAUGHT ON FIRE. FIRE WAS CAUSED BY EXHAUST PIPE BEING TOO CL...