NHTSA Complaint #11220806 — 2014 KENWORTH T680
ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 11220806 |
| Vehicle | 2014 KENWORTH T680 |
| Component | ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 480,050 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | WA |
Consumer Description
A VIBRATION IS FELT DURING WARM UP AND BECOMES VERY NOTICEABLE AFTER SHIFTING INTO 8TH GEAR. IF THE AIR COMPRESSOR KICKS IN WHILE THE ENGINE IS BELOW 1300 RPMS THIS ALSO INCREASES THE VIBRATION , AGAIN REAL BAD SHIFTING INTO 8TH AND AIR COMPRESSOR RUNNING .NOTE: I JUST BOUGHT THIS TRUCK FROM KENWORTH SALES COMPANY , SALT LAKE CITY, UT I AINT EVEN PUT 2,000 MILES ON THE TRUCK, WHAT KINDA OF DECEITFUL ETHICS VIOLATIONS ARE PRACTICED FROM THIS DEALERSHIP?
Related Complaints for the 2014 KENWORTH T680
Other ENGINE Complaints
Recent Complaints for the 2014 KENWORTH T680
#11450487
ELECTRICAL SYSTEM
This Truck Was Park. The Paccar Engine MX13 and Chassis Harness from the Driver Side Shortaged, causing a Fire in the...
#11315835
FUEL/PROPULSION SYSTEM
APPARENTLY THERE IS A FAILURE OF THE FUEL PUMP IN MOST MODELS OF THIS CUMMINS ISX15 MOTOR, THA WHEN IT DOES FAIL, SHU...
#11099334
ELECTRICAL SYSTEM
BUNK WIRING HARNESS IS SHORTING OUT CAUSING TRUCK TO NOT BE ABLE TO SHUT OFF WITH THE KEY....AND ALSO CAUSING PROBLEM...
#11099334
ELECTRONIC STABILITY CONTROL (ESC)
BUNK WIRING HARNESS IS SHORTING OUT CAUSING TRUCK TO NOT BE ABLE TO SHUT OFF WITH THE KEY....AND ALSO CAUSING PROBLEM...
#10958529
POWER TRAIN
THIS TRUCK IS A MISBUILD FROM THE FACTORY ON THE BRAKE SYSTEM PLUMBING. I AM CONCERNED OTHER UNITS MAY ALSO HAVE BEEN...