NHTSA Complaint #11080568 — 2003 MONACO COACH DYNASTY
ENGINE AND ENGINE COOLING issue reported to NHTSA
Complaint Details
| ODI Number | 11080568 |
| Vehicle | 2003 MONACO COACH DYNASTY |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | 155,957 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | TX |
Consumer Description
WE HAD A HORRIFYING EXPERIENCE DUE TO A MASSIVE FUEL LEAK ON JAN 12, 2018, LESS THAN THREE MONTHS AFTER SERVICE HAD BEEN HAD BEEN COMPLETED AT CUMMINS CROSSPOINT ON OCT 18, 2017. CUMMINS HAD REPLACED THE ENGINE HARNESS ON THE ISL-400 ENGINE OF OUR MONACO MOTORHOME AS A RESULT OF AN EARLIER FUEL LEAK THEY DISCOVERED IN MAY OF 2017. CUMMINS CROSSPOINT ASSURED US, AFTER WE ASKED AT LEAST THREE TIMES THAT ALL FUEL LEAKAGE ISSUES HAD BEEN CORRECTED. WE DO NOT KNOW IF THE FUEL LEAK ON JAN 12TH WAS THE RESULT OF IMPROPER INSPECTION OR POOR WORKMANSHIP BY CUMMINS CROSSPOINT, OR IF IT IS THE RESULT OF DESIGN FLAWS OR INITIAL MANUFACTURING ERROR; HOWEVER THERE APPEARS TO BE NO OTHER EXPLANATION. AS WE EVENTUALLY LEARNED, THE MASSIVE LEAK WAS A RESULT OF THE #5 FUEL LINE BECOMING TOTALLY DISCONNECTED AS WE DROVE. IT APPEARS THAT THIS LEAK OCCURRED OVER THE LAST MILE OR SO AS WE NOTICED THE ENGINE WAS NOT RUNNING CORRECTLY AND WE EXITED THE IINTERSTATE A SAT DISABLED WAITING FOR A TOW TRUCK THAT ARRIVED THAT EVENING. AS WE SAT WE SAID A PRAYER OF THANKS THAT WE'D NOT BEEN INJURED OR KILLED BY A FIRE THAT MIGHT HAVE OCCURRED. AT NO TIME DURING THE INCIDENT WAS THERE A DASH WARNING LIGHT TO INDICATE THAT ANYTHING WAS WRONG. CLEARLY CUMMINS CROSSPOINT FAILED ON THREE SERVICE OCCASIONS, TO PROPERLY IDENTIFY AND RECTIFY THE FUEL LEAK WHICH THEY KNEW EXISTED, SINCE THEY REPLACED WIRING WHICH THEY TOLD US HAD BEEN DAMAGED BY SAID FUEL LEAK. THIS IS A FAILURE WHICH NEVER SHOULD HAVE HAPPENED TO A CUMMINS ?MILLION MILE? ENGINE. COMPRESSION CONNECTORS SHOULD BE ENGINEERED SO AS NOT TO FALL APART BY THEMSELVES. AFTER THREE FAILURES OF THE CUMMINS ORGANIZATION TO RESOLVE THE ISSUE, WE HAD THE REPAIR DONE BY AN INDEPENDENT DIESEL ENGINE REPAIR SHOP. WHEREAS THE FUEL LEAK HAS BEEN REPAIRED THE ORIGINAL DESIGN FLAW IN THE CUMMINS ISL400 ENGINE REMAINS.
Related Complaints for the 2003 MONACO COACH DYNASTY
Recent Complaints for the 2003 MONACO COACH DYNASTY
#10465649
TIRES
GOODYEAR G670 RV TIRE: "RIVERING"- TYPE TREAD WEAR LEADS TO STEERING PULL AFTER LESS THAN 25,000 MILES OF USE. FRONT...
#10370383
EQUIPMENT:RECREATIONAL VEHICLE/TRAILER
WE RECEIVED A RECALL LETTER FROM NORCOLD REGARDING THE 1200 SERIES REFRIGERATOR IN OUR RV. THE RECALL LETTER HAS TO ...
#10154362
SERVICE BRAKES, AIR:DISC:CALIPER
BRAKE CALIPER BOLT CAUSES TIRE DEFLATION THE BOLT (CAP SCREW) ON TOP OF THE FRONT LEFT CALIPER ON MY 2003 MONACO DYN...
#10154362
TIRES:VALVE
BRAKE CALIPER BOLT CAUSES TIRE DEFLATION THE BOLT (CAP SCREW) ON TOP OF THE FRONT LEFT CALIPER ON MY 2003 MONACO DYN...