NHTSA Complaint #10723259 — 2006 KIA SEDONA
SUSPENSION issue reported to NHTSA
Complaint Details
| ODI Number | 10723259 |
| Vehicle | 2006 KIA SEDONA |
| Component | SUSPENSION |
| Date of Incident | |
| Date Filed | |
| Mileage | 85,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | OH |
Consumer Description
I WAS DRIVING WITH MY 3 YOUNG CHILDREN IN MY 2006 KIA SEDONA WHEN ANOTHER DRIVER PULLED OUT IN FRONT OF ME CAUSING ME TO APPLY THE BRAKES, AT WHICH TIME I LOST CONTROL OF THE VAN WHICH NEARLY ROLLED OVER. I LATER LEARNED THAT WHEN THE BRAKES WERE APPLIED, THE DRIVER'S SIDE LOWER CONTROL ARM COMPLETELY BROKE DUE TO RUST WHICH IS WHAT CAUSED ME TO LOSE CONTROL. THANKFULLY, THE VAN CAME TO A STOP BUT ONLY BECAUSE THE WHEEL BROKE AND BECAME LODGED. HAD THIS ACCIDENT HAPPENED ON THE FREEWAY, THERE WOULD HAVE BEEN SERIOUS INJURIES OR FATALITIES. CORROSION ON THE FRONT LOWER CONTROL ARM WAS PART OF A RECALL ISSUED IN NOVEMBER 2013. ON FEBRUARY 20, 2014 (BEFORE I OWNED THE VAN), THE VAN WAS TAKEN TO A KIA SERVICE CENTER FOR SERVICE RELATED TO THE RECALL. A RUSTPROOF COATING WAS APPLIED TO THE REAR CONTROL ARMS AND THE FRONT WERE VISUALLY INSPECTED AND DETERMINED TO BE FINE. JUST OVER A YEAR LATER THE PART DETERMINED TO BE "SAFE," BROKE FROM SIMPLY APPLYING THE BRAKES WHICH VERY EASILY COULD HAVE RESULTED IN DEVASTATING CONSEQUENCES. I CONTACTED KIA ON MAY 22, 2015. AS OF JUNE 3, 2015 (13 DAYS SINCE THE INCIDENT) I AM STILL AWAITING A RESPONSE FROM KIA AS TO WHAT CORRECTIVE ACTION THEY WILL TAKE. I FEAR FOR THE SAFETY OF MY FAMILY TO EVER DRIVE THIS VEHICLE AGAIN.
Related Complaints for the 2006 KIA SEDONA
Other SUSPENSION Complaints
#11516462
FRAME RUSTED -OUT ALLOWING RIGHT FRONT WHEEL A -FRAME TO COME LOOSE. ALLOWING WHEEL TO MOVE REARWARD INTO WHEELWELL ...
#11426055
Driving slowly out of parking lot a loud bang was heard. Scraping noise was heard from under van, drove about 25 yard...
#11350941
PASSENGER SIDE RR CONTROL ARM RUSTED THROUGH WHICH CAUSED IT TO BEND AND CAUSED RR TIRE TO FOLD INWARD. HAD TO REPLA...
#11341959
LEFT REAR LOWER CONTROL ARM HAD RUSTED AND BROKE WHILE BACKING UP IN A PARKING LOT.
#11315668
WHILE ATTEMPTING TO ENTER TRAFFIC FROM OUR DRIVEWAY UPON ACCELERATION THE STEERING WHEEL SHOOK AND A LOUD "THUD" WAS ...