NHTSA Complaint #10471041 — 2010 FORD EXPEDITION
ELECTRICAL SYSTEM issue reported to NHTSA
Complaint Details
| ODI Number | 10471041 |
| Vehicle | 2010 FORD EXPEDITION |
| Component | ELECTRICAL SYSTEM |
| Date of Incident | |
| Date Filed | |
| Mileage | 41,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | MN |
Consumer Description
THE FAILURES OCCURRED OVER A 3 DAY PERIOD. THE MOTOR QUIT WHILE IDLING FOR LESS THAN 5 MINUTES IN A RESTAURANT PARKING LOT. INITIALLY, IT WOULD NOT EVEN TURN OVER. HOWEVER, AFTER SEVERAL ATTEMPTS IT DID RE-START. THE MOTOR STALLED AGAIN ABOUT 90 MINUTES LATER WHILE GOING 30 MILES PER HOUR. WHILE COASTING, WE TURNED OFF THE MAIN STREET (WITH GREAT DIFFICULTY) - THE POWER STEERING, BRAKES ETC. NO LONGER WORKING. IT STARTED AFTER MANY FUTILE ATTEMPTS. WE HEADED TOWARDS A FORD DEALERSHIP AND THE MOTOR STALLED AGAIN, NOW ON A BUSY FREEWAY - AFTER MULTIPLE ATTEMPTS, WHILE COASTING, THE MOTOR DID RESTART. THAT DEALERSHIP HAD THE VEHICLE FOR 24 HOURS BUT FOUND NOTHING. THEIR COMMENT: "IT IS RUNNING FINE NOW - IT IS LIKELY ELECTRONIC - TAKE IT TO YOUR LOCAL DEALER". WE LEFT THE NEXT DAY FOR THE 240 MILE TRIP HOME. WE WERE ON A MAJOR FREEWAY DURING "RUSH HOUR" EXTREMELY CONGESTED TRAFFIC (DUE TO CONSTRUCTION) WHEN THE MOTOR STALLED ONCE AGAIN. WE HAD JUST MERGED FROM 2 LANES TO 1 AND MY HUSBAND WAS ABLE TO "MUSCLE THE VEHICLE" INTO THE RIGHT LANE AND ONTO THE SHOULDER. THIS TIME, AFTER MULTIPLE ATTEMPTS, NOTHING. WE WERE STRANDED ON A MAJOR FREEWAY WITH 2 DOGS AND ENDLESS 65 MPH TRAFFIC FLYING BY. AFTER UNLOADING OUR DOGS INTO THE MIDST OF THIS DANGEROUS SITUATION, OUR 2010 EXPEDITION WAS LOADED ONTO A FLATBED TRUCK TO BE HAULED THE 65 MILES REMAINING TO OUR HOME (AND THE DEALERSHIP WHERE WE PURCHASED THE VEHICLE). AFTER 3 DAYS OF DIAGNOSTICS FOUND NOTHING, SOMEONE AT FORD (DETROIT) SUGGESTED THE "WIGGLE-WIRE" TEST BEFORE, AS A LAST RESORT, REPLACING THE COMPUTER SYSTEM. WITH THE ENGINE RUNNING, THE WIRES WERE WIGGLED UNTIL ONE ACTUALLY STOPPED THE ENGINE. IT HAD BEEN "CRIMPED", AS WIRES WERE "MERGED" FROM MANY TO A FEW AT THE FACTORY, EVENTUALLY CAUSING A SHORT. THE STALLING ENGINE COULD EASILY HAVE RESULTED IN AN HORRIFIC ACCIDENT. AND, I AM NOT CONVINCED IT IS TRULY "FIXED".
Related Complaints for the 2010 FORD EXPEDITION
Other ELECTRICAL SYSTEM Complaints
#11482932
Interior A/c blower motor short. A/c stops and starts by itself with smell of wiring melting or burnt.
#11258661
I ATTEMPTED TO ROLE MY WINDOW UP WHILE DRIVING AND IT STOPPED WORKING. THE WINDOW WILL NOT ROLL UP OR DOWN AND IS STU...
#11140157
TRANSMISIN PROBLEM BERY NOISE WHEN DRIVING AND PRESS GAS. SOMETIMES WHEN IS PARKED IT MOVES LIKE 12" . AC ALWAYS A ...
#11019268
WHEN WE TOUCH THE BRAKES, FROM STARTING POSITION OR WHEN IN MOTION, THE ELECTRICAL COMPONENTS IN THE DASH FLASH AND F...
#10985088
TL* THE CONTACT OWNS A 2010 FORD EXPEDITION. WHILE THE VEHICLE WAS AT A STANDSTILL, THE FRONT DRIVER AND PASSENGER SI...
Recent Complaints for the 2010 FORD EXPEDITION
#11608372
UNKNOWN OR OTHER
My vehicle will just shut off. No warning. No lights. It shuts off, I have to turn on my hazards, put it in park and ...
#11432724
UNKNOWN OR OTHER
Drivers side airbag did not deploy when the car was in an accident. The passenger side did even though there was no p...
#11378057
UNKNOWN OR OTHER
A/C COMPRESSOR CLUTCH AND PULLEY SEPERATED A/C COMPRESSOR SEIZED UP SERPENTINE BELT GOT DAMAGED FROM THE SEIZE. TRUCK...
#11246618
POWER TRAIN
TL* THE CONTACT OWNS A 2010 FORD EXPEDITION. THE CONTACT STATED THAT WHILE THE VEHICLE WAS IDLING WITH THE PARK ENGAG...
#11222778
ENGINE
FIRST INCIDENT IN MARCH 2019 FROM PARKED POSITION, PUT CAR IN DRIVE AND IT "RACED" OUT OF CONTROL, TRIED TO BRAKE AND...