NHTSA Complaint #10411471 — 1999 FORD F-150
ENGINE AND ENGINE COOLING issue reported to NHTSA
Complaint Details
| ODI Number | 10411471 |
| Vehicle | 1999 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | 25,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | NV |
Consumer Description
I PURCHASED MY 1999 FORD F-150 4X 4 WITH A TRITON 5.4 V-8 ENGINE USED. THE ENGINE HAD APPROXIMATELY 140,000 WHEN I PURCHASED IT. I ONLY DRIVE IT TO AND FROM WORK IN LAS VEGAS, NV (APPROXIMATELY 25 MILES ROUND TRIP) AT SPEEDS BELOW 50 MPH. THE ENGINE BLEW THE BACK PLUG AT 163,000. BECAUSE IT WAS THE BACK PLUG THE LABOR TO REPAIR WAS HIGH (PULL THE ENGINE). THE DIFFERENCE IN PUTTING HELICOILS (ALL EIGHT PLUGS) IN AND A NEW ENGINE WAS NOT THAT MUCH DIFFERENCE SO I ORDER A LONG BLOCK FULL ENGINE FROM FORD WITH STIPULATIONS IT CORRECTED THE DESIGN FLAW. THE ENGINE COST ALMOST $7000 WHEN ALL WAS DONE AND COMPLETE. FORD WARRANTY THE ENGINE 3 YEARS AND 75,000 MILES. I FIGURED THIS CORRECTED THE ISSUES WITH THE SPARK PLUGS BLOWING OUT. WELL AT THE 4 YEAR POINT AND APPROXIMATE 25,000 MILES THE NEW ENGINE BLEW A PLUG. FORD AND THE DEALER (WHOM WE PURCHASED THE ENGINE FROM) SAY IT IS OUR PROBLEM. THE DEALER (PARTS MANAGER) ACTUALLY SAID SINCE I WAS NOT A FREQUENT CUSTOMER AND HAD PURCHASED THE TRUCK USED THEY DID NOT SEE A WAY TO HELP. I HAVE RESEARCHED THIS ISSUE ON THE INTERNET AND BELIEVE IT IS DESIGN FLAW IN THE HEAD. I AM IN THE PROCESS OF HAVING STEEL INSERTS PUT IN ALL OF THE SPARK PLUG HOLES SO I MIGHT GET USE OUT OF A HEFTY INVESTMENT IN A MOTOR WITH A KNOWN ISSUE WHICH FORD WILL NOT BACK. I OWN A FORD CROWN VICTORY, A MERCURY MARQUIS LS, AND THE F-150 TRUCK . . . THESE ARE THE LAST VEHICLES I WILL OWN FROM FORD. *TR
Related Complaints for the 1999 FORD F-150
Other ENGINE AND ENGINE COOLING Complaints
#10455648
TL* THE CONTACT OWNS A 1999 FORD F-150. THE CONTACT STATED THAT THE EXHAUST MANIFOLD STARTED BREAKING AWAY FROM THE V...
#10437895
STARTED THE TRUCK UP AN BLAST OFF! DONT KNOW WHERE THE PLUG WENT BUT IT WAS GONE AFTER I HEARD A LOUD BANG. *KB *TR
#10432469
CYLINDER 5 SPARK PLUG BLEW OUT WHILE DRIVING, WRECKING THE THREADING IN THE SPARK PLUG HOLE AND THE COIL. *TR
#10427009
IN MAY WAS AT A STOP LIGHT WHEN THE LIGHT TURNED GREEN I ACCELERATED AND THE PLUG BLEW AT SECONDS LATER I GOT IT TOWE...
#10405786
HAVE HAD A SPARK PLUG EJECTED TWICE NOW WITHIN 3000 MILES. AFTER SOME RESEARCH THIS SEEMS TO BE A COMMON PROBLEM WITH...
Recent Complaints for the 1999 FORD F-150
#11534217
VEHICLE SPEED CONTROL
The contact owned a 1999 Ford F-150. The contact stated that he had parked the vehicle and was standing outside of th...
#11404509
ENGINE
TL* THE CONTACT OWNED A 1999 FORD F-150. THE CONTACT STATED WHILE THE VEHICLE WAS PARKED AT HIS RESIDENCE, THE VEHICL...
#11360722
ENGINE
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722
EXTERIOR LIGHTING
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722
POWER TRAIN
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...