NHTSA Complaint #10361624 — 2003 FORD F-250 SD
POWER TRAIN:AUTOMATIC TRANSMISSION issue reported to NHTSA
Complaint Details
| ODI Number | 10361624 |
| Vehicle | 2003 FORD F-250 SD |
| Component | POWER TRAIN:AUTOMATIC TRANSMISSION |
| Date of Incident | |
| Date Filed | |
| Mileage | 103,906 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | CO |
Consumer Description
TRANSMISSION COOLER SUPPLY LINE (METAL TUBING NOT HOSE ELEMENT) DEVELOPED A LEAK DUE TO LONG TERM CONTACT WITH THE ENGINE SUPPORT FRAME CROSSMEMBER. LONG TERM CONTACT RESULTED IN A .25 INCH WIDE X .5 INCH LONG FLAT AREA WORN INTO TUBE WALL WITH A PIN HOLE SIZE PENETRATION THRU THE TUBE WALL. FLUID PRESSURE INSIDE THE TUBE IN COMBINATION WITH THE PIN HOLE SIZE PENETRATION RESULTED IN A SPRAYING LEAK FROM THE TUBE WHICH COATED THE UNDERCARRIAGE OF THE TRUCK AND THE TRAILER THAT WAS IN TOW AT THE TIME OF FAILURE. THE BRAKING SURFACES ON ALL FOUR WHEELS OF THE TRUCK WERE COATED WITH TRANSMISSION FLUID. THE LOW VOLUMETRIC FLOWRATE OF THE LEAK ALLOWED FOR CONTINUED OPERATION OF THE VEHICLE FOR SEVERAL HOURS (AT NIGHT ON FAIRLY LEVEL TERRAIN) WITHOUT ANY INDICATION OF THE ONGOING LEAKAGE. THIS ALLOWED FOR THE UNDERCARRIAGE OF THE VEHICLE INCLUDING THE BRAKING SURFACES TO BE COATED WITH FLUID. THE LEAKAGE WAS IDENTIFIED WHEN THE TRANSMISSION TEMPERATURE GAUGE INDICATED HOT WHILE TRANSITIONING TETON PASS FROM JACKSON WYOMING. INSPECTION OF THE TUBING INSTALLATION REVEALED THAT THE DIRECT CAUSE OF THE LEAKAGE WAS THE AFORE MENTIONED LONG TERM CONTACT WITH THE ENGINE SUPPORT FRAME CROSSMEMBER. THE ROOT CAUSE OF THE ISSUE IS EITHER DESIGN TOLERANCE FOR THE TUBING INSTALLATION OR INCORRECT INSTALLATION OF THE TUBING AT ORIGINAL ASSEMBLY. THE CLAMPING PROVISION DESIGNED INTO THE TUBING INSTALLATION (ATTACHED TO THE SIDE OF THE ENGINE BLOCK ADJACENT TO THE OIL PAN) IN COMBINATION WITH THE INSUFFICIENT LENGTH OF THE TUBING SECTION CROSSING OVER THE ENGINE SUPPORT FRAME CROSSMEMBER RESULTED IN PRELOADED CONTACT BETWEEN THE TUBE AND THE FORWARD EDGE OF THE CROSSMEMBER. AT THE TIME OF THE FAILURE NO REPLACEMENT PARTS WERE AVAILABLE SO THE DAMAGED SECTION OF THE TUBING WAS REMOVED AND REPLACED WITH HIGH PRESSURE HYDRAULIC HOSE. THE REMOVED SECTION OF TUBING WAS RETAINED AND IS AVAILABLE FOR INSPECTION. THE TRUCK REMAINS IN THE TEMPORARY REPAIRED CONDITION AT THIS TIME. *TR
Related Complaints for the 2003 FORD F-250 SD
Other POWER TRAIN:AUTOMATIC TRANSMISSION Complaints
#10437474
VEHICLE HAS 7.3 LITER DIESEL ENGINE AND THE FORD 4R100 AUTOMATIC TRANSMISSION AND 4 WHEEL DRIVE. TRANSMISSION FAILED...
#10357350
TL* THE CONTACT OWNS A 2003 FORD F250 SD. THE CONTACT STATED THAT THE VEHICLE WAS SHUT OFF WITH THE SHIFTER IN PARK ...
#10247115
2003 FORD F-250 (ONLY 50,000 MILES) HAD MAJOR TRANSMISSION FAILURE. HOUSING CRACKED AND THERE IS NO WAY TO REPAIR....
#10146878
2003 F-250 SD 4X4 CC 5.4 L GAS AUTO TRANSMISSION. WHEN THE TRUCK IS STARTED IT LURCHES FORWARD. THIS HAS BEEN HAPPENI...
#10133756
DT: A SHIFT CABLE BROKE ON JUNE 5, 2005. CONTACTED THE DEALER, THEY FIXED IT. HAD SEVERAL ISSUES WITH THE TRUC...
Recent Complaints for the 2003 FORD F-250 SD
#11230742
FUEL/PROPULSION SYSTEM
TL* THE CONTACT OWNS A 2003 FORD F-250 SD. WHILE THE VEHICLE WAS PARKED, THE CONTACT NOTICED THAT THE FUEL TANK WAS H...
#11150844
FUEL/PROPULSION SYSTEM
THE REAR FUEL TANK STRAP FAILED WHILE TRAVELING ON A STATE HIGHWAY.
#10935359
WHEELS
I HAVE AMERICAN EAGLE - 20 " EAGLE ALLOY WHEELS. THEY ARE APPROXIMATELY 24 MONTHS OLD. THIS SUMMER A SPOKE CRACKED A...
#10871769
ELECTRICAL SYSTEM
I HAVE HAD SEVERAL PROBLEMS WITH THE SPARK PLUGS BLOWING OUT OF MOTOR AND BREAKING COIL CAUSING IT TOO LEAK FUEL VAPO...
#10871769
UNKNOWN OR OTHER
I HAVE HAD SEVERAL PROBLEMS WITH THE SPARK PLUGS BLOWING OUT OF MOTOR AND BREAKING COIL CAUSING IT TOO LEAK FUEL VAPO...