NHTSA Complaint #10356671 — 1997 FORD E-350
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Fire
Complaint Details
| ODI Number | 10356671 |
| Vehicle | 1997 FORD E-350 |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 37,414 miles |
| Crash | No |
| Fire | Yes |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | IL |
Consumer Description
MY V10 FORD E-350 MOTOR HAD A HEAD FAILURE AND A SPARK PLUG BLEW OUT WHILE DRIVING. A FIRE STARTED IN THE ENGINE COMPARTMENT AND THE EXPLOSION SOUND CREATED A PANIC AND STARTLED RESPONSE THAT ALMOST LEAD TO A VEHICLE CRASH. THE VEHICLE WAS TOWED TO A REPAIR FACILITY AND THEY WERE FAMILIAR WITH THE PROBLEM. THEY WORK ON FLEET VEHICLES REGULARLY AND THEY STATED THEY HAVE SEEN THIS PROBLEM MANY TIMES BEFORE. THE ALUMINUM HEAD OF THE ENGINE WAS TOO WEAK TO HOLD ON TO THE SPARK PLUG AND THAT LEAD TO THE EXPLOSION, FIRE, AND DAMAGE. THE SHOP INFORMED ME THAT THIS COULD VERY LIKELY HAPPEN AGAIN BECAUSE OF THE DEFECTIVE DESIGN OF THE ENGINE AND IF I AM TRAVELING WITH MY FAMILY I COULD BE LEFT STRANDED, POSSIBLE A VERY DANGEROUS PART OF THE HIGHWAY WHILE DRIVING STEEP OR DANGEROUS ROADS. IF THE VEHICLE CATCHES ON FIRE AGAIN IT COULD EXPLODE IF THE GAS LINE IGNITES. THIS ONE CYLINDER COST $800 TO FIX BUT NOW I HAVE 9 OTHER ONES TO WORRY ABOUT. I WAS NOT ABLE TO FIND A CURRENT RECALL BUT THERE WILL HAVE TO BE ONE ISSUED TO ENSURE THE SAFETY OF ANY AMERICAN DRIVING A FORD VEHICLE WITH THIS ENGINE. AFTER RESEARCHING THE INTERNET I HAVE FOUND LITERALLY THOUSANDS OF DIFFERENT PEOPLE STATING SIMILAR SCENARIOS. *TR
Related Complaints for the 1997 FORD E-350
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10252281
THE #3 SPARK PLUG ON MY '97 FORD E-350 VAN BLEW OUT (ABOUT 1 YEAR AFTER THE PLUGS WERE CHANGED) WHILE STARTING TO DRI...
#10245191
1997 FORD E350 V-10 ENGINE VAN BLEW OUT THE NUMBER 4 SPARK PLUG. LOUD POPPING SOUND FOLLOWED BY LOSS OF POWER AND STR...
#10082416
THE MOTOR HOME ENGINE OPERATED FINE WHILE WE WERE ON AN EXTENDED 1700 MILE TRIP. THE GAUGES REGISTERED NORMAL. WE CH...
#10002719
SPARK PLUG WAS BLOWN OUT OF THE ALUMINUM HEAD OF AN E-350 FORD V-8 VORTEX ENGINE. MECHANICS I HAVE SPOKEN TO HAVE RE...
#745253
OIL FILTER HOUSING UNIT BOLTED TO LEFT SIDE OF TRITON V-10 ENGINE FELL OFF THE ENGINE AFTER BOLTS WHICH HELD THE HOUS...