NHTSA Complaint #10325264 — 2002 FORD MUSTANG GT
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10325264 |
| Vehicle | 2002 FORD MUSTANG GT |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 46,383 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | OK |
Consumer Description
I OWN A 2002 FORD MUSTANG GT WITH A 2-VALVE 4.6L ENGINE WITH ONLY 46K MILES. AROUND 1 APR 10 I STARTED HEARING A DISTINCT TICKING NOISE FROM THE ENGINE. NOT BEING THAT MECHANICALLY INCLINED, I ASSUMED SOME LIFTERS NEEDED ADJUSTING; SO, I BRUSHED THE NOISE OFF. ON 10 APR 10 I WAS DRIVING ON THE INTERSTATE WHEN I HEARD A LOUD BANG AND THEN SOUNDS THAT PATTED LIKE A HARLEY RUNNING OUT OF GAS. MY CHECK ENGINE LIGHT FLASHED SEVERAL TIMES. FORTUNATELY, I WAS ONLY 2 MILES FROM HOME; SO, I SPUTTERED THE REST OF THE WAY. AS I HAVE A DIAGNOSTIC TOOL, I CHECKED THE CODE AND IT READ THE #3 CYLINDER WAS MISS FIRING. I CALLED MY MECHANIC AND HE TOLD ME TO CHANGE THE SPARK PLUGS. ONCE I FIGURED OUT HOW TO GET ALL THAT DONE, I REMOVED THE COIL FROM THE CYLINDER AND IT WAS SHREDDED WITH THE COIL DANGLING. I EXTRACTED THE SPARK PLUG WITH NO RESISTANCE BECAUSE IT WAS JUST SITTING IN THE HOLE. TO MY SURPRISE, IT WAS THE ORIGINAL SPARK PLUG THAT CAME WITH THE CAR. I TRIED TO PUT IN A NEW SPARK PLUG, BUT IT WOULD NOT TIGHTENED AT ALL. I ATTEMPTED SEVERAL TIMES AND EVEN TRIED TO MAKE IT CROSS-THREAD, BUT IT WOULD NOT TAKE. WHEN I TOOK A GOOD LOOK AT THE SPARK PLUG, I SAW WHERE THE BOTTOM THREE THREADS WERE SMASHED FLAT AND THE METAL THAT YOU GAP WAS MASHED AGAINST THE ELECTRIC DIODE. I CALLED BOB MOORE FORD IN OKC AND THE SERVICE WRITER, GERRY, TOLD ME THERE WERE NO RECALLS FOR THAT EVENT. I ASKED HIM WHAT COULD HAVE CAUSED IT AND HE RESPONDED IMPROPERLY TORQUED SPARK PLUGS. WHEN I TOLD HIM IT WAS THE FACTORY PLUG, HE SAID THEN HOT RODDING MUST HAVE CAUSED IT. I TOLD HIM ITS MY WIFE'S CAR AND THE CAR DOESN'T TAKE ANY ABUSE. I ASKED HOW MUCH BOB MOORE CHARGES TO DO A HELICOIL AND HE SAID $500. I LET HIM GO. I ENDED UP TAKING IT TO A MECHANIC SHOP AND GETTING THE CYLINDER RE-THREAD FOR WHOLE LOT LESS AND WHOLE LOT BETTER ATTITUDE. HOPEFULLY, IT HOLDS. *TR
Related Complaints for the 2002 FORD MUSTANG GT
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10302355
SPARK PLUGS EJECTING OUT OF CYLINDER HEAD ON MY 2002 FORD MUSTANG GT. HAD ONE BLOW OUT 1 YEAR AGO AND NOW ANOTHER ON ...
#10258876
I HAVE A 2002 FORD MUSTANG GT THAT I BOUGHT NEW. I WAS DRIVING TO WORK ON 2/16/09 & I HEARD A LOUD SOUND LIKE SOMEONE...
#10188074
I OWN A 2002 FORD MUSTANG GT. I BOUGHT THIS CAR BRAND NEW FROM THE DEALER, I HAVE NEVER HAD ANY MECHANICAL PROBLEMS W...
#10173017
CAR WILL BOG/ HAVE LITTLE POWER ON ACCELERATION THEN YOU WILL FEEL THE CAR PICK UP AND GO. ALSO, WHEN ACCELERATING FR...
#10133620
COMING OUT OF A RED LIGHT, I HEARD THE SOUND OF COMPRESSED AIR BEING BLOWN OUT. I IMMEDIATELY PARKED IN A LOCAL STORE...
Recent Complaints for the 2002 FORD MUSTANG GT
#11061482
SEAT BELTS
I RECENTLY WAS TRAVELING ON THE INTERSTATE LATE AFTER WORK ON INTERSTATE 10 AT 60 MPH WHEN I WAS STRUCK FROM BEHIND ...
#11061482
STRUCTURE:BODY
I RECENTLY WAS TRAVELING ON THE INTERSTATE LATE AFTER WORK ON INTERSTATE 10 AT 60 MPH WHEN I WAS STRUCK FROM BEHIND ...
#11061482
WHEELS
I RECENTLY WAS TRAVELING ON THE INTERSTATE LATE AFTER WORK ON INTERSTATE 10 AT 60 MPH WHEN I WAS STRUCK FROM BEHIND ...
#10885859
ELECTRONIC STABILITY CONTROL (ESC)
THE ABS ELECTRONIC STABILITY CONTROL WARNING LIGHT HAS COME ON. IT CANNOT BE TURNED OFF. THERE HAS BEEN NO PROBLEM WI...