NHTSA Complaint #10229984 — 2001 FORD F SERIES
ENGINE AND ENGINE COOLING issue reported to NHTSA
Complaint Details
| ODI Number | 10229984 |
| Vehicle | 2001 FORD F SERIES |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | 19 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | CT |
Consumer Description
WE OWN A MOTOR HOME, BUILT ON A FORD INCOMPLETE VEHICLE CHASSIS, POWERED BY A FORD V-10 TRITON ENGINE. THE FIRST ENGINE BEGAN TO SPIT OUT SPARK PLUGS AFTER REACHING 75,000 MILES ON THE ODOMETER. THIS OCCURRED ON FRIDAY, JANUARY 27, 2006, ABOUT FORTY MILES EAST OF KINGMAN, ARIZONA. AFTER SPENDING MONEY TO GET THE PROBLEM DIAGNOSED AT A GOODYEAR DEALERSHIP IN KINGMAN, ARIZONA, WE HAD TO ORDER A SPECIAL REPAIR KIT FROM BARIL ENGINE REBUILDING COMPANY IN GREEN BAY, WISCONSIN, PAYING FOR THE SHIPPING BOTH WAYS. A MECHANIC RESLEEVED THE CYLINDER. AS I HAD TO MAKE A SPEAKING ENGAGEMENT, WE HAD TO DRIVE FOR CLOSE TO 1,000 MILES WITH WRETCHED FUMES AND HORRID NOISE. THE SECOND SPARK PLUG WAS SPIT OUT ON FRIDAY, FEBURARY 10, 2007. AS I HAD ANOTHER SPEAKING ENGAGEMENT, WHICH IS HOW I MAKE MY LIVING, WE HAD TO DRIVE TO PENSACOLA, FLORIDA, AND THENCE LAFAYETTE, LOUISIANA, BEFORE ANOTHER REPAIR KIT WAS RENTED TO BE USED BY YET ANOTHER MECHANIC. THE THIRD SPARK PLUG WAS SPIT OUT TWO WEEKS LATER, ON MONDAY, FEBRUARY 26, 2007, AS WE WERE DRIVING FROM PENSACOLA TO LAFAYETTE. WE RENTED THE TOOL KIT FROM BARIL ENGINE REBUILDING COMPANY ONCE AGAIN. THIS ORIGINAL FORD V-10 TRITON ENGINE DIED ON THURSDAY, APRIL 19, 2007, ON INTERSTATE 80/94 JUST EAST OF MILE MARKER 160. TWO CYLINDERS HAD LOST COMPRESSION ENTIRELY. NO ONE AT TERRY FORD LINCOLN MERCURY IN PEOTONE, ILLINOIS, COULD EXPLAIN WHY THIS HAD HAPPENED. WE HAD TO RAISE $9,000 TO PAY FOR A NEW ENGINE AND ITS INSTALLATION. THE ENGINE HAD BEEN WELL MAINTAINED. THE REPLACEMENT ENGINE HAS ALSO BEEN MAINTAINED WELL. DESPITE THIS FACT, HOWEVER, THE ENGINE SPIT OUT ITS FIRST SPARK PLUG, JUST 19,000 MILES AND THIRTEEN MONTHS, EIGHT DAYS AFTER ITS INSTALLATION, AN INCIDENT THAT OCCURRED THIS AFTERNOON, WEDNESDAY, JUNE 3, 2008, AT EXIT 22 OF THE NEW YORK STATE THRUWAY IN SELKIRK, NEW YORK. *TR
Related Complaints for the 2001 FORD F SERIES
Other ENGINE AND ENGINE COOLING Complaints
#10446872
SPARK PLUG BLEW OUT OF ENGINE CAUSING FAILURE. ENGINE. *TR FIRE
#10284397
2001 FORD F150 CAUGHT FIRE IN THE MIDDLE OF THE NIGHT AND WAS COMPLETELY DESTROYED. VEHICLE HAD NOT CRANKED IN OVER 2...
#10253733
ON MULTIPLE OCCASIONS I HAVE BEEN DRIVING AND HEARD A LOUD BANG AND FELT THE MOTOR STARTING TO SHAKE AND LOSS OF POWE...
#10235880
#3 SPARK BLEW OUT OF ENGINE HEAD AND BROKE SPARK PLUG COIL IN THE PROCESS. THIS WAS AN ORIGINAL FACTORY INSTALLED SP...
Recent Complaints for the 2001 FORD F SERIES
#10928820
ENGINE
SPARK PLUG EJECTED FROM THE ENGINE BLOCK, AS VEHICLE WAS MOVING ON A HIGHWAY. DISABLED, NEEDED A TOW. REPAIR VERY E...
#10916233
ENGINE
SPARK PLUG BLOWN OUT OF HEAD. SPARK PLUG #7 BLEW OUT 9 MONTHS AGO. NOW PLUG #8 BLEW OUT. MECHANIC SAYS IT'S DUE T...
#10908389
ENGINE
THE SPARKPLUG BLEW OUT FOR THE SECOND TIME. THE FIRST TIME WAS ABOUT 9 MONTHS AGO. RUNNING FINE THEN ABOUT 40 MPH THE...
#10735102
STRUCTURE:BODY
I HAVE A 2001 FORD F-150 THAT I PURCHASED BRAND NEW IN 2001. I HAVE NOTICED THAT THE ENTIRE FRAME IS RUSTED AND I AM...
#10725641
ELECTRICAL SYSTEM
TURN SIGNAL ARE NOW SPORADIC. UPON INVESTIGATING I FOUND THAT WHEN THE TILT IS ENGAGED AND LOWERED THE TURN SIGNALS W...