NHTSA Complaint #10188672 — 2000 BUICK LESABRE
ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:EMISSION CONTROL:CATALYTIC CONVERTOR issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10188672 |
| Vehicle | 2000 BUICK LESABRE |
| Component | ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:EMISSION CONTROL:CATALYTIC CONVERTOR |
| Date of Incident | |
| Date Filed | |
| Mileage | 64,800 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | WI |
Consumer Description
MARCH 30TH, 2007 CAR RAN ROUGH AND SERVICE ENGINE SOON LIGHT CAME ON. A BAD ODOR ALSO WAS PERMEATING INTO THE CAR WHILE GOING DOWN THE ROAD. CAR WENT BACK TO THE DEALER ON THE 31ST AND THEY HAD THE CAR UNTIL THE 3RD OF APRIL. I DROVE THE CAR ABOUT TWO MILES AND THE CAR DID EXACTLY WHAT IT WAS DOING BEFORE WHEN I DROPPED IT OFF. I DROPPED THE CAR BACK OFF THE NEXT DAY ON THE 4TH THEY HAD IT UNTIL SATURDAY THE 7TH. THEY SAID THEY CHANGED THE SPARK PLUGS AND THAT WAS WHAT WAS WRONG. I DROVE THE CAR AND EVERYTHING WAS FINE UNTIL FRIDAY THE 13TH. I WENT TO START THE CAR IN THE MORNING AND IT WOULDN'T START RIGHT AWAY. WHEN IT DID IT STUNK SO BAD FROM TO MUCH GAS FROM TRYING TO START IT. I RAN IT THAT DAY AND IT RAN ROUGH A FEW TIMES AND DIDN'T CALL THE DEALER. I LOANED MY CAR TO MY BROTHER FRIDAY NIGHT AND I DIDN'T TELL HIM ABOUT THE STARTING PROBLEM OR THE RUNNING ROUGHLY. HE WENT TO START THE CAR AFTER WORK ON SATURDAY MORNING AND IT WOULDN'T START RIGHT AWAY FOR HIM. HE GOT IT GOING AND HE TOLD ME THAT IT RAN ROUGH AND BUCKED AND JERKED. WHEN HE BROUGHT THE CAR BACK TO ME IT SAT IN MY DRIVEWAY FOR ABOUT FOUR HOURS. MY WIFE WENT TO START IT AND PUT IT INTO THE GARAGE FOR THE NIGHT AND SHE COULD NOT GET IT TO START SHE HAD TO COME AND GET ME TO GET IT GOING. I CALLED THE DEALER ON MONDAY THE 16TH AND THEY TOLD ME TO BRING IT IN THE NEXT DAY. I DID SO AND THEY SENT IT TO A GARAGE TO HAVE IT LOOKED AT. ABOUT 2:00 ON WEDNESDAY THE 18TH I STOPPED TO SEE IF IT WAS FIXED AND THEY SAID IT WAS THAT IT WAS THE SPARK PLUGS AGAIN THE GARAGE DIDN'T PUT PREMIUM PLUGS IN. THEY TOLD ME THAT THEY WASHED MY CAR FOR MY INCONVENIENCES. ALSO THE FUEL MILEAGE ON THE CAR WAS 20 MPG WHICH IS EXTREMELY LOW IT SHOULD GET 30-32 MPG. I TOLD THEM THIS ALSO. SO I GOT THE CAR BACK AND TODAY THE 19TH OF APRIL THE CAR IS HAVING PROBLEMS RUNNING PROPERLY. I RETURNED THE CAR AND THEY WONT CALL ME AT ALL. I FEARED MY CHILDREN'S SAFETY IN THIS CAR. *JB
Related Complaints for the 2000 BUICK LESABRE
Other ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:EMISSION CONTROL:CATALYTIC CONVERTOR Complaints
#10136985
7/17/2000: STALLED 2X IN TRAFFIC W/315 MILES ON IT; REPLACED WIRE HARNESS & FUSES; 4/9/02:LEAK-REPLACED UPPER MANIFO...
#10073422
VEHICLE WAS HAVING A PROBLEM WITH THE CATALYTIC CONVERTER. THE MFR. WAS UNABLE TO REPAIR THE CATALYTIC CONVERTER BECA...
#885524
FUEL TANK AND SENDING LINES NEED TO BE REPLACED DUE TO O-RINGS IMPROPERLY FITTED ON FUEL PUMP. IN JULY 2000, VEH...
Recent Complaints for the 2000 BUICK LESABRE
#11706263
FUEL/PROPULSION SYSTEM
the 2000 Buick Lesabre is a wonderful car basically a tank with the 3800 SERIES II you cant go wrong but the tiny lit...
#11706263
VEHICLE SPEED CONTROL
the 2000 Buick Lesabre is a wonderful car basically a tank with the 3800 SERIES II you cant go wrong but the tiny lit...
#11676853
FORWARD COLLISION AVOIDANCE: ADAPTIVE CRUISE CONTROL
The plastic pice holding the throttle lines snapped off and my cable went under my bracket and it took off I destroye...
#11676853
VEHICLE SPEED CONTROL
The plastic pice holding the throttle lines snapped off and my cable went under my bracket and it took off I destroye...
#11463054
FUEL/PROPULSION SYSTEM
I started my car in the morning, per my usual routine. After a few seconds, I heard a very loud bang and the car stal...