NHTSA Complaint #10163438 — 1999 FORD MUSTANG GT
ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10163438 |
| Vehicle | 1999 FORD MUSTANG GT |
| Component | ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE |
| Date of Incident | |
| Date Filed | |
| Mileage | 92,400 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | CA |
Consumer Description
(7/23/06) 1999 FORD MUSTANG GT, 4.6L BLEW SPARK PLUG FOR THE THIRD TIME NOW. THE FIRST TIME WAS BACK IN 2005 WHILE DRIVING ON THE 15 FREEWAY HEADING SOUTH AT ABOUT 8:00 PM. STOP TO GET GAS AND UPON STARTING THE VEHICLE TO CONTINUE MY WAY HOME IT MADE LOUD POP AND THEN CONTINUED TO POP, POP, POP. AT FIRST I THOUGHT I HAD AN EXHAUST MANIFOLD PROBLEM, BUT UPON THE REPAIR SHOP INSPECTION OF THE VEHICLE THEY NOTED THAT THE NUMBER ONE SPARK PLUG HAD BLEW OUT OF THE PISTON. THEY REPAIRED IT FOR ABOUT $ THE SECOND TIME WAS ABOUT 6 MONTHS AGO WHEN THE NUMBER TWO SPARK PLUG (ALL THIS BEING ON THE DRIVERS SIDE) BLEW OUT. NO DAMAGE TO THE THREADS AND A NEW SET OF SPARK PLUGS WERE PUT INTO THE VEHICLE ALL AROUND. THEN ON SUNDAY EVENING, JULY 23RD 2006, THE SAME NUMBER 2 SPARK PLUG BLEW OUT AGAIN; THIS TIME TAKING ALL THE THREADS WITH IT. I HAD TO HAVE THE CAR TOWED TO MY PLACE OF RESIDENCE AND NOW I AM IN THE PROCESS OF FINDING A REPAIR SHOP TO RE-THREAD THE PISTON. I AM SURE THEY WILL HAVE TO GET A NEW COIL AS WELL; SINCE IT BROKE OFF AT THE PLACE OF WERE IT IS BOLTED TO THE HEAD. I CALLED FORD MOTOR COMPANY ON TUESDAY, JULY 25TH 2006 AND SPOKE TO CUSTOMER SERVICE REP. AND BASICALLY WAS GIVEN A NOT OUR PROBLEM ATTITUDE. THIS IS APPALLING THAT SUCH A LARGE COMPANY AS FORD WILL NOT ACKNOWLEDGE THE PROBLEM AND FIX IT! I AM A SINGLE MOTHER AND CAN NOT AFFORD TO HAVE MY CAR FIXED AT OVER $3000.00! I AM NOT HAPPY WITH FORD AND WILL NOT BUY FROM THEM AGAIN. I WAS A HUGE FORD FAN; WHEN ANYONE WOULD TRY TO DISCREDIT THEM I WOULD BACK THEM ALL THE WAY! NOT ANY MORE THEY DON'T BACK THEIR CUSTOMERS. I GUESS FORD MOTOR COMPANY HAS NO LOYALTY TO THEIR CUSTOMERS WHAT SO EVER! SO I SHALL NO LONGER BE LOYAL TO THEM. I WILL BE BUYING A CHEVY OR OTHER VEHICLE THAT HAS NO ASSOCIATION WITH THE FORD NAME, AS SOON AS THIS IS FIXED. SHE'S BEING TRADED IN ASAP! *JB
Related Complaints for the 1999 FORD MUSTANG GT
Other ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE Complaints
Recent Complaints for the 1999 FORD MUSTANG GT
#10611188
ENGINE
THE CAR WAS BUILT WITH A PLASTIC INTAKE MANIFOLD. THE MANIFOLD BEGAN LEAKING AT THE THERMOSTAT HOUSING AND THEN THE H...
#10330287
ENGINE AND ENGINE COOLING
CAR LUNGES IN DRIVE OR REVERSE BEFORE ACCELERATOR IS DEPLOYED. *TR
#10276302
ENGINE AND ENGINE COOLING:ENGINE
HEARING A EXHAUST LEAK LIKE NOISE AND AROUND THE SPARK PLUG THERE IS AIR COMING OUT OF THE HEADS CAUSING THEM TO EVEN...