NHTSA Complaint #10611188 — 1999 FORD MUSTANG GT

ENGINE issue reported to NHTSA

Check any vehicle history by VIN - Free vehicle history report

Complaint Details

ODI Number 10611188
Vehicle 1999 FORD MUSTANG GT
Component ENGINE
Date of Incident
Date Filed
Mileage 142,000 miles
Crash No
Fire No
Injuries 0
Deaths 0
Vehicle Towed No
State OH

Consumer Description

THE CAR WAS BUILT WITH A PLASTIC INTAKE MANIFOLD. THE MANIFOLD BEGAN LEAKING AT THE THERMOSTAT HOUSING AND THEN THE HEATER HOSE CONNECTION ON THE INTAKE MANIFOLD SUDDENLY BROKE. I NOW HAVE TO HAVE THE ENTIRE INTAKE MANIFOLD REPLACED BECAUSE OF POOR DESIGN AND MATERIAL SELECTION. FORD KNEW OF THE PROBLEM BUT REFUSES TO ADDRESS THE ISSUE AND HOPES IT WILL JUST GO AWAY. THEY SHOULD REIMBURSE THE OWNERS OF THE VEHICLES FOR REPAIRS THAT WERE DUE TO POOR DESIGN AND MATERIALS USED TO MAKE THIS PART. *TR

Related Complaints for the 1999 FORD MUSTANG GT

Recent Complaints for the 1999 FORD MUSTANG GT

#10447185 ENGINE AND ENGINE COOLING SPARK PLUG BLEW OUT OF AN ALREADY FIXED HEAD!!! *TR
#10330287 ENGINE AND ENGINE COOLING CAR LUNGES IN DRIVE OR REVERSE BEFORE ACCELERATOR IS DEPLOYED. *TR
#10330287 VEHICLE SPEED CONTROL CAR LUNGES IN DRIVE OR REVERSE BEFORE ACCELERATOR IS DEPLOYED. *TR
#10276302 ENGINE AND ENGINE COOLING:ENGINE HEARING A EXHAUST LEAK LIKE NOISE AND AROUND THE SPARK PLUG THERE IS AIR COMING OUT OF THE HEADS CAUSING THEM TO EVEN...
#10247316 ENGINE AND ENGINE COOLING SLOWING DOWN FOR A STOP SIGN WHEN THE 3 RD SPARK PLUG BLEW OUT ON THE PASSENGER SIDE OF MY 1999 MUSTANG GT WITH A 4.6...
Check any vehicle history by VIN - Free vehicle history report