NHTSA Complaint #10151838 — 1994 BUICK SKYLARK
ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10151838 |
| Vehicle | 1994 BUICK SKYLARK |
| Component | ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE |
| Date of Incident | |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | WI |
Consumer Description
I OWN A 1994 BUICK SKYLARK. IT DEVELOPED A COOLANT LEAK. I HAD THE HEATER CORE REPLACED ON ADVISE OF A MECHANIC THAT UNTIL RECENTLY WAS AT A GM DEALERSHIP. IT STILL LEAKED WHEN THE ENGINE WAS COLD. IT WAS THEN DETERMINED THAT IT WAS THE WATER PUMP SO I HAD THAT REPLACED. IT STILL LEAKED. NOW I HAVE TO HAVE THE LOWER INTAKE MANIFOLD GASKET REPLACED AT AN ESTIMATED COST OF $660.00. I HAVE CONTACTED GM DEALERSHIPS AND INDEPENDENT MECHANICS IN REGARDS TO THE MANIFOLD GASKET AND HAVE BEEN TOLD THAT THE PROBLEM WITH THE GASKET IS THAT IT IS A DEFECTIVE DESIGN AND THAT MANY LOWER INTAKE MANIFOLD GASKETS HAVE BEEN REPLACED ON THE SKYLARKS BECAUSE OF THIS DEFECT. APPARENTLY GM DECIDED TO USE A PLASTIC GASKET AS OPPOSED TO THE PAPER COMPOSITE GASKET AND THIS IS THE CAUSE OF SO MANY VEHICLES HAVING TO HAVE THIS GASKET REPLACED. I STRONGLY FEEL THAT GM SHOULD HAVE ISSUED A RECALL ON THIS PROBLEM WHEN IT BECAME APPARENT THAT IT WAS DUE TO A DEFECT IN DESIGN. *JB
Related Complaints for the 1994 BUICK SKYLARK
Recent Complaints for the 1994 BUICK SKYLARK
#10507409
ELECTRICAL SYSTEM
ON 11/14/2012 I BOUGHT AN EXCIDE CAR BATTERY FROM NATIONAL AUTO IN BANGOR, PA. BATTERY RAN FOR ABOUT 2 MOS. THEN STA...
#10441798
STEERING
TILT STEERING WHEEL ASSEMBLY FAILED AND STEERING WHEEL BECAME DETACHED FROM THE STEERING COLUMN. UPON FURTHER INSPEC...
#10166235
ELECTRICAL SYSTEM:IGNITION
DT*: THE CONTACT STATED WHILE DRIVING 25 MPH, THE VEHICLE ENGINE HESITATED, THEN STALLED COMPLETELY. THE VEHICLE LO...
#10166235
ENGINE AND ENGINE COOLING
DT*: THE CONTACT STATED WHILE DRIVING 25 MPH, THE VEHICLE ENGINE HESITATED, THEN STALLED COMPLETELY. THE VEHICLE LO...
#10107463
POWER TRAIN:AXLE ASSEMBLY
WHILE DRIVING 30 MPH, THE CONSUMER WOULD HEAR A CLUNKING NOISE. THE DEALERSHIP REPAIRED THE FRONT DRIVER SIDE AXLE. P...