NHTSA Complaint #10136508 — 1999 FORD F-150

ENGINE AND ENGINE COOLING:ENGINE:GASOLINE issue reported to NHTSA

Check any vehicle history by VIN - Free vehicle history report
Vehicle Towed

Complaint Details

ODI Number 10136508
Vehicle 1999 FORD F-150
Component ENGINE AND ENGINE COOLING:ENGINE:GASOLINE
Date of Incident
Date Filed
Mileage 45,000 miles
Crash No
Fire No
Injuries 0
Deaths 0
Vehicle Towed Yes
State AK

Consumer Description

MANUFACTURING DEFECT - PLUG THREAD FAILURE VEHICLE IS A 1999 FORD F-150 4X WITH 5.4L TRITON AND APPROX. 45,000 MILES. WHILE UNAGGRESSIVELY ACCELLERATING AT NORMAL HIGHWAY SPEEDS THE ENGINE LOST POWER AND A LOUD POPPING SOUND COULD BE HEARD. THE VEHICLE WAS IMMEDIATELY PULLED TO THE SIDE OF THE HIGHWAY, TURNED OFF, AND TOWED TO A REPAIR FACILITY. NO INJURY OR CRASH OCCURRED. INVESTIGATION INDICATED A SPARK PLUG AND COIL HAD BEEN EJECTED FROM THE HEAD. THE PLUG WAS THE 2ND FROM THE FRONT ON PASSENGER SIDE. THE THREADS IN THE HEAD WERE STRIPPED SUCH THAT A NEW SPARK PLUG COULD NOT BE SEATED. A HELICOIL WAS INSTALLED FOR APPROX. $300 AND LOSS OF VEHICLE FOR A WEEK, BUT IT FAILED AFTER APPROXIMATELY 3 MONTHS. THIS FAILURE WAS EVIDENCED BY ENGINE MISFIRE, POWER LOSS AND SLUGGISHNESS. INVESTIGATION REVEALED THAT SAME PLUG WAS NOT FIRING, AND WAS NOT ABLE TO BE REMOVED BECAUSE THE HELICOIL THREADS WERE ALSO STRIPPED. THE HEAD WAS REPLACED AT A COST OF $3,626 WITH AND ADDITIONAL 2 WEEKS LOST VEHICLE USE (2 COMPARABLE QUOTES FROM REPUTABLE AUTO REPAIR PROVIDERS WERE OBTAINED). REPAIR TIME WAS LONGER THAN USUAL AS THE PART HAD TO BE ORDERED FROM OUT-OF-STATE AND EXPEDITED SHIPPING WAS DEEMED TOO EXPENSIVE. AT THIS TIME, HOWEVER, THE ENGINE MISFIRES CONTINUOUSLY AT IDLE AND FREQUENTLY AT HIGHWAY SPEEDS. THE VEHICLE IS CURRENTLY IN THE SHOP FOR A 3RD TIME TO INVESTIGATE THIS CONTINUING CONDITION. *NM

Related Complaints for the 1999 FORD F-150

Other ENGINE AND ENGINE COOLING:ENGINE:GASOLINE Complaints

#10223646 1999 FORD F150 5.4L V8 BLEW OUT THE NUMBER FOUR (4) SPARK PLUG LOCATED ON THE PASSENGER SIDE IN THE REAR. PERSONAL R...
#10187636 HAVE A 1999 F150 THAT HAS A FIX RECORDED FOR THE HEAD GASKET, BUT HAS NO RECALL. EVEN THOUGH FORD KNOWS THERE IS A FA...
#10182774 1999 FORD F-150 SPARK PLUGS BLOWING OUT. *NM
#10139994 I WAS DRIVING MY FAMILY DOWN A WINDING MAJOR MOUNTAIN HIGHWAY IN MY 1999 FORD F150 TRUCK (5.4L V-8, 117400 MILEAGE) W...
#10137884 1999 F 150. THE ENGINE SPIT THE SPARK PLUG OUT AND DAMAGED THE HEAD,COIL, WIRING AND HOOD. *JB

Recent Complaints for the 1999 FORD F-150

#11534217 VEHICLE SPEED CONTROL The contact owned a 1999 Ford F-150. The contact stated that he had parked the vehicle and was standing outside of th...
#11404509 ENGINE TL* THE CONTACT OWNED A 1999 FORD F-150. THE CONTACT STATED WHILE THE VEHICLE WAS PARKED AT HIS RESIDENCE, THE VEHICL...
#11360722 ENGINE LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722 EXTERIOR LIGHTING LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722 POWER TRAIN LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
Check any vehicle history by VIN - Free vehicle history report