NHTSA Complaint #10136508 — 1999 FORD F-150
ENGINE AND ENGINE COOLING:ENGINE:GASOLINE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10136508 |
| Vehicle | 1999 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING:ENGINE:GASOLINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 45,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | AK |
Consumer Description
MANUFACTURING DEFECT - PLUG THREAD FAILURE VEHICLE IS A 1999 FORD F-150 4X WITH 5.4L TRITON AND APPROX. 45,000 MILES. WHILE UNAGGRESSIVELY ACCELLERATING AT NORMAL HIGHWAY SPEEDS THE ENGINE LOST POWER AND A LOUD POPPING SOUND COULD BE HEARD. THE VEHICLE WAS IMMEDIATELY PULLED TO THE SIDE OF THE HIGHWAY, TURNED OFF, AND TOWED TO A REPAIR FACILITY. NO INJURY OR CRASH OCCURRED. INVESTIGATION INDICATED A SPARK PLUG AND COIL HAD BEEN EJECTED FROM THE HEAD. THE PLUG WAS THE 2ND FROM THE FRONT ON PASSENGER SIDE. THE THREADS IN THE HEAD WERE STRIPPED SUCH THAT A NEW SPARK PLUG COULD NOT BE SEATED. A HELICOIL WAS INSTALLED FOR APPROX. $300 AND LOSS OF VEHICLE FOR A WEEK, BUT IT FAILED AFTER APPROXIMATELY 3 MONTHS. THIS FAILURE WAS EVIDENCED BY ENGINE MISFIRE, POWER LOSS AND SLUGGISHNESS. INVESTIGATION REVEALED THAT SAME PLUG WAS NOT FIRING, AND WAS NOT ABLE TO BE REMOVED BECAUSE THE HELICOIL THREADS WERE ALSO STRIPPED. THE HEAD WAS REPLACED AT A COST OF $3,626 WITH AND ADDITIONAL 2 WEEKS LOST VEHICLE USE (2 COMPARABLE QUOTES FROM REPUTABLE AUTO REPAIR PROVIDERS WERE OBTAINED). REPAIR TIME WAS LONGER THAN USUAL AS THE PART HAD TO BE ORDERED FROM OUT-OF-STATE AND EXPEDITED SHIPPING WAS DEEMED TOO EXPENSIVE. AT THIS TIME, HOWEVER, THE ENGINE MISFIRES CONTINUOUSLY AT IDLE AND FREQUENTLY AT HIGHWAY SPEEDS. THE VEHICLE IS CURRENTLY IN THE SHOP FOR A 3RD TIME TO INVESTIGATE THIS CONTINUING CONDITION. *NM
Related Complaints for the 1999 FORD F-150
Other ENGINE AND ENGINE COOLING:ENGINE:GASOLINE Complaints
#10223646
1999 FORD F150 5.4L V8 BLEW OUT THE NUMBER FOUR (4) SPARK PLUG LOCATED ON THE PASSENGER SIDE IN THE REAR. PERSONAL R...
#10187636
HAVE A 1999 F150 THAT HAS A FIX RECORDED FOR THE HEAD GASKET, BUT HAS NO RECALL. EVEN THOUGH FORD KNOWS THERE IS A FA...
#10182774
1999 FORD F-150 SPARK PLUGS BLOWING OUT. *NM
#10139994
I WAS DRIVING MY FAMILY DOWN A WINDING MAJOR MOUNTAIN HIGHWAY IN MY 1999 FORD F150 TRUCK (5.4L V-8, 117400 MILEAGE) W...
#10137884
1999 F 150. THE ENGINE SPIT THE SPARK PLUG OUT AND DAMAGED THE HEAD,COIL, WIRING AND HOOD. *JB
Recent Complaints for the 1999 FORD F-150
#11534217
VEHICLE SPEED CONTROL
The contact owned a 1999 Ford F-150. The contact stated that he had parked the vehicle and was standing outside of th...
#11404509
ENGINE
TL* THE CONTACT OWNED A 1999 FORD F-150. THE CONTACT STATED WHILE THE VEHICLE WAS PARKED AT HIS RESIDENCE, THE VEHICL...
#11360722
ENGINE
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722
EXTERIOR LIGHTING
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722
POWER TRAIN
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...