NHTSA Complaint #10133928 — 1995 DODGE STEALTH
POWER TRAIN:TRANSFER CASE (4-WHEEL DRIVE) issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10133928 |
| Vehicle | 1995 DODGE STEALTH |
| Component | POWER TRAIN:TRANSFER CASE (4-WHEEL DRIVE) |
| Date of Incident | |
| Date Filed | |
| Mileage | 129,240 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | TX |
Consumer Description
DT: THE CALLER RECEIVED MANUFACTURER'S RECALL B17 CONCERNING TRANSFER CASE. AFTERIT HAD BEEN FIXEDHEARD A GRINDING NOISE. WHILE DRIVING AT 30 MPH THE REAR TIRES LOCKED AND IT JERKED THE VEHICLE. NOW IT MAKES A NOISE ALL THE TIME. DEALER SAID THE CALLER WOULD HAVE TO PAY TO HAVE IT LOOKED AT AGAIN. MANUFACTURER SAID TO TAKE IT TO A DEALER TO SEE IF IT WAS THE TRANSFER CASE OR SOMETHING ELSE AND HE WOULD HAVE TO PAY FOR IT. *AK
Related Complaints for the 1995 DODGE STEALTH
Recent Complaints for the 1995 DODGE STEALTH
#10203297
SEAT BELTS:FRONT:RETRACTOR
WHEN THE SEAT BELT IS PULLED ON IT DOES NOT RETRACT, LEAVING ENOUGH SLACK IN THE BELT THAT IF AN ACCIDENT WERE TO OCC...
#10158327
SEAT BELTS:FRONT:RETRACTOR
FAILURE IN RETRACTING OF DRIVER'S SIDE SEAT BELT. HAVE TO RETRACT SEAT BELT MANUALLY. *JB
#10087219
POWER TRAIN:AUTOMATIC TRANSMISSION
CONSUMER COMPLAINED THAT AUTOMATIC TRANSMISSION HAD AN ONGOING PROBLEM WITH SHIFTING INTO NEUTRAL WHILE DRIVING AT H...
#10040790
POWER TRAIN:MANUAL TRANSMISSION:COLUMN SHIFT ASSEMBLY
WHILE TRAVELING AT 70 MPH VEHICLE MADE A LOUD POPPING NOISE. DRIVER TEMPORARILY LOST CONTROL OF VEHICLE, BUT WAS ABLE...
#752619
POWER TRAIN:AUTOMATIC TRANSMISSION
THE TRANSMISSION FAILED. THE ENGINE JUST REVVED AND WOULD NOT GO INTO REVERSE. TRANSMISSION HAD TO BE TOTALLY REBUILT...