NHTSA Complaint #10070998 — 1999 DODGE INTREPID
ENGINE AND ENGINE COOLING issue reported to NHTSA
Complaint Details
| ODI Number | 10070998 |
| Vehicle | 1999 DODGE INTREPID |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | 84,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | KS |
Consumer Description
IN THE FALL OF 2001, WE BOUGHT A CERTIFIED USED CAR FROM CONTINENTAL AUTO MALL. IT IS A 1999 DODGE INTREPID. A SERVICE AGREEMENT ON THE CAR WAS ALSO PURCHASED. THE FOLLOWING HAS THEREAFTER TAKEN PLACE: THE TIMING CHAIN IDLER BROKE IN MARCH OF 2002. CONTINENTAL FIXED THE CAR UNDER SERVICE AGREEMENT. 67 MILES LATER, THE CAR DIED WITH MY DAUGHTER AND WIFE 7 MILES FROM HOME. IT HAD TO BE TOWED BACK TO CONTINENTAL AUTO MALL. WE ASKED WHAT HAPPENED AND WERE TOLD THAT THE OIL PUMP SCREEN WAS PLUGGED UP. WE ASKED FROM WHAT AND THEY SAID FROM THE FIBERS FROM THE TIMING CHAIN IDLER. FROM MY FATHER'S LIMITED EXPERIENCE IN MECHANIC WORK, THE OIL PUMP SCREEN BEING CLOGGED FROM FIBERS FROM THE CHAIN IDLER MEANT THAT THE ENGINE WAS NOT FLUSHED. SO FOR 67 MILES AFTER THE TIMING CHAIN WAS REPAIRED, THESE FIBERS WERE GOING THROUGH THE ENGINE EVENTUALLY CLOGGING THE OIL PUMP SCREEN. THE OIL PRESSURE MUST HAVE BECOME SO LOW THAT A SAFETY SWITCH SHUT OFF THE ENGINE. WE WERE TOLD THAT THE SAFETY SWITCH SHUT THE ENGINE OFF SO THAT THE LOW PRESSURE WOULDN?T FURTHER DAMAGE THE ENGINE. REPAIRS WERE AGAIN MADE BY CONTINENTALS SHOP. UNTIL THESE TWO INCIDENTS, WE WERE VERY HAPPY WITH THE CAR. AFTER WE GOT THE CAR BACK AFTER THE ENGINE SHUT OFF, THIS IS WHAT WE NOTICED: 1. THE ENGINE DIDN?T SEEM AS QUIET WHEN RUNNING. 2. IT NEEDED A QUART OF OIL THE FIRST WEEK. 3. BETWEEN OIL CHANGES, WE HAD TO ADD OIL 2-3 TIMES. BEFORE IT HAD NEVER USED ANY OIL. OTHER THAN ADDING OIL, WE DIDN?T HAVE ANY PROBLEMS UNTIL THE POWER STEERING BELT IDLER BROKE THE 2ND WEEK IN AUGUST OF 2003. OUR MECHANIC, JOHN RICKMAN OF JOHN?S AUTO IN GIRARD, SHOWED US THE BRACKET FROM THE IDLER. THE BRACKET IS A FIVE-BOLT BRACKET, WHICH HAD ONLY TWO BOLTS IN IT, AND YOU CAN SEE WHERE THOSE TWO BOLTS HAVE BEEN WORKING. ON AUGUST 20, 2003, I PARKED THE CAR AT A FLOWER SHOP IN GIRARD. I CAME BACK TO THE CAR TO GO HOME AND THE CAR WOULDN?T START.
Related Complaints for the 1999 DODGE INTREPID
Other ENGINE AND ENGINE COOLING Complaints
#10397772
1999 DODGE INTREPID COOLING SYSTEM AND ENGINE TROUBLE
#10381480
I PURCHASED A 1999 DODGE INTREPID. I HAVE COMPLETE SERVICE RECORDS FOR THE VEHICLE SHOWING THAT ON AVG. THE OI...
#10350489
1999 DODGE INTREPID - 2.7 LITRE ENGINE. RPM'S PERIODICALLY DROPPED (LIKE THE ENGINE WAS GOING TO CUT OUT), BLACK SMO...
#10346846
MY DODGE INTREPID WAS SERVICED AT KEYSTONE DODGE OR BUD BROWN DODGE IN OVERLAND PARK, KS FOR EVERY OIL CHANGE. AT JU...
#10339984
TL* THE CONTACT OWNS 1999 DODGE INTREPID. WHILE THE CONTACT WAS DRIVING APPROXIMATELY 40 MPH, THE ENGINE REVVED EXCE...
Recent Complaints for the 1999 DODGE INTREPID
#11104994
ELECTRICAL SYSTEM
THE AIR CONDITIONING AND HEAT WENT OUT IN CAR. WINDOWS POWER KEEP GETTING STUCK.
#11074157
AIR BAGS
TL* THE CONTACT OWNS A 1999 DODGE INTREPID. WHILE DRIVING APPROXIMATELY 75 MPH, THE AIR BAGS DEPLOYED WITHOUT WARNING...
#10979716
EXTERIOR LIGHTING
I BOUGHT THIS 1999 DODGE INTREPID FROM CLIFFS USED CARS SALES TWO MONTHS AGO. EVERYTHING SEEMED GOOD ONE MONTH OR LES...
#10979716
SEATS
I BOUGHT THIS 1999 DODGE INTREPID FROM CLIFFS USED CARS SALES TWO MONTHS AGO. EVERYTHING SEEMED GOOD ONE MONTH OR LES...
#10979716
SUSPENSION
I BOUGHT THIS 1999 DODGE INTREPID FROM CLIFFS USED CARS SALES TWO MONTHS AGO. EVERYTHING SEEMED GOOD ONE MONTH OR LES...