NHTSA Complaint #10050756 — 2000 BUICK LESABRE
ENGINE AND ENGINE COOLING:COOLING SYSTEM issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10050756 |
| Vehicle | 2000 BUICK LESABRE |
| Component | ENGINE AND ENGINE COOLING:COOLING SYSTEM |
| Date of Incident | |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | FL |
Consumer Description
COOLANT LEAKAGE FROM COOLANT RESEVOIR INTO AIR INTAKE MANIFOLD. IT IS OBVIOUS THAT ENGINE COOLANT DRAWN INTO CYLYNDER HEAD CAN HAVE NUMEROUS RESULTS DAMAGING TO THE OPERATION AND LONGEVITY OF THE ENGINE. FURTHER THE LOSS OF COOLANT FORM THE RESEVOIR CAN RESULT IN INADEQUATE ENGINE COOLING AND HIGH AND DESTRUCTIVE ENGINE TEMPERATURES. WHILE THERE WAS NO OBSERVED EVIDENCE OF COOLANT LOSS BEFORE GMC RECALL TO "TIGHTEN THROTTLE BODY BOLTS", THE LOSS OF COOLANT ACCELERATED AFTER THE UNSUCCESSFUL EFFORT TO ELIMINATE COOLANT LOSS. THAT THIS PROBLEM HAS BEEN PRESENT SINCE EARLY IN 2000 MODEL OF THE BUICK LESABERS IS EVIDENCED BY COMPLAINTS AND SERVICE REPORTS. THE RECALL PROGRAM OF SUMMER 2003 WAS AN INADEQUATE SOLUTION TO THE PROBLEM. IN ADDITION TO THIS HISTORY, THE EXISTANCE OF LONG STANDING PROBLEM IS CONFIRMED BY GMC'S RECALL IN THE SUMMER OF 2003. MY COMPLAINT IS HEIGHTENED BY THE FACT THAT BOTH THE DEARLER AND GM REFUSED TO INVESTIGATE THE COOLANT LOSS OBSERVED AFTER THE RECALL AS A PART OF THE RECALL AND USED THE EXPIRY OF MY ORIGINAL WARRANTY AFTER THE RECALL ANNOUNCEMENT AND ALSO AFTER THE COMPLETION OF RECALL SERVICING WITHOUT FULLY CHARGING ME FOR THE INVESTIGATION AND REQUIRED REMEDIAL WORK TO RESOLVE THE COOLANT LEAKAGE MALFUNCTION. DURING MY RESEARCH INTO THIS SITUATION I ENCOUNTERED A "MR GOOD WRENCH" WHO WORKED IN SERVICE DEPARTMENT OF A LARGE BUICK DEALER. WHILE DISCUSSING THE THROTTLE BODY LEAKAGE, HE COMMENTED THE "BUICK HAS AN EVEN BIGGER PROBLEM WITH THE "PLASTIC SECTION OF THE INTAKE MANIFOLD WHICH IS ENCOUNTERING FREQUENT CRACKING OF THIS SECTION OF THE MANIFOLD RESULTING IN LOSS OF COOLANT AND MAJOR ENGINE OPERATION DIFFICULTIES. SOUNDS TO ME THIS PROBLEM WHICH IS EVEN MORE DAMAGING AND EXPENSIVE TO CONSUMER THAN THE THROTTLE BODY LEAKAGE MERITS AN INVESTIGATION.*AK
Related Complaints for the 2000 BUICK LESABRE
Other ENGINE AND ENGINE COOLING:COOLING SYSTEM Complaints
#10181767
HEATER ONLY BLEW COLD AIR. UPPER INTAKE LEAKING COOLANT. UPPER INTAKE REPLACED COULD HAVE CAUSED ENGINE TO FREEZE...
#10093541
2000 BUICK LESABRE LTD APPROXIMATELY.(1)MONTH AFTER PURCHASE VEHICLE STALLED IN TRAFFIC WHILE COMING TO A STOP OR AT ...
#10010198
UPPER INTAKE MANIFOLD HAD TO BE REPLACED DUE TO A COOLANT LEAK. THIS TYPE REPAIR APPEARS TO BE VERY UNUSUAL FOR THI...
#10005533
TWO COMPLAINTS. ONE-COOLANT LEAKING ON HOT ENGINE PARTS FROM DEFECTIVE INTAKE MANIFOLD PLENUM. TWO- CAR STALLS ON OCC...
#10000074
LEAKING COOLANT LED TO REPLACEMENT OF INTAKE MANIFORD ON 2000 BUICK LESABRE WITH 3.8L ENGINE COSTING $540. NEWSPAPER...
Recent Complaints for the 2000 BUICK LESABRE
#11706263
FUEL/PROPULSION SYSTEM
the 2000 Buick Lesabre is a wonderful car basically a tank with the 3800 SERIES II you cant go wrong but the tiny lit...
#11706263
VEHICLE SPEED CONTROL
the 2000 Buick Lesabre is a wonderful car basically a tank with the 3800 SERIES II you cant go wrong but the tiny lit...
#11676853
FORWARD COLLISION AVOIDANCE: ADAPTIVE CRUISE CONTROL
The plastic pice holding the throttle lines snapped off and my cable went under my bracket and it took off I destroye...
#11676853
VEHICLE SPEED CONTROL
The plastic pice holding the throttle lines snapped off and my cable went under my bracket and it took off I destroye...
#11463054
FUEL/PROPULSION SYSTEM
I started my car in the morning, per my usual routine. After a few seconds, I heard a very loud bang and the car stal...