NHTSA Complaint #10041289 — 1999 FORD MUSTANG GT
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10041289 |
| Vehicle | 1999 FORD MUSTANG GT |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 56,650 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | CA |
Consumer Description
CAR STALLS WHEN SLOWING TO A STOP AND HAS HAPPENED SEVERAL TIMES. TOOK THE CAR TO FORD AND CLEANED THE THROTTLE BODY AND REFLASHED THE COMPUTER. THE PROBLEM CAME BACK SEVERAL DAYS LATER AND CHANGED THE IDLE AIR CONTROL VALVE YET THE PROBLEM STILL ARISES. WHEN SLOWING TO A STOP THE RPM DROP TO 500 RPM AND THEN BOUNCED BACK UP TO AN IDLE AT 700 RPM. OTHER TIMES THAT IT WILL DROP BELOW 500 RPM, AND THE CAR STARTS TO STALL. *LA
Related Complaints for the 1999 FORD MUSTANG GT
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10276302
HEARING A EXHAUST LEAK LIKE NOISE AND AROUND THE SPARK PLUG THERE IS AIR COMING OUT OF THE HEADS CAUSING THEM TO EVEN...
#10247316
SLOWING DOWN FOR A STOP SIGN WHEN THE 3 RD SPARK PLUG BLEW OUT ON THE PASSENGER SIDE OF MY 1999 MUSTANG GT WITH A 4.6...
#10212665
1999 FORD MUSTANG GT APPEARS TO HAVE CRACK IN PLASTIC INTAKE SYSTEM, AND IS LOSING COOLANT. PREVIOUSLY OWNED A 1997...
#10174364
THERE WAS A SLIGHT TICKING NOISE COMING FROM ENGINE BAY THAT I THOUGHT WAS AN EXHAUST LEAK. EVENTUALLY THE SPARK PLU...
#10164047
FORD SPARK PLUG BLOW OUT ON 1999 FORD MUSTANG GT 4.6 L MOTOR. *NM
Recent Complaints for the 1999 FORD MUSTANG GT
#10611188
ENGINE
THE CAR WAS BUILT WITH A PLASTIC INTAKE MANIFOLD. THE MANIFOLD BEGAN LEAKING AT THE THERMOSTAT HOUSING AND THEN THE H...
#10330287
ENGINE AND ENGINE COOLING
CAR LUNGES IN DRIVE OR REVERSE BEFORE ACCELERATOR IS DEPLOYED. *TR
#10247316
ENGINE AND ENGINE COOLING
SLOWING DOWN FOR A STOP SIGN WHEN THE 3 RD SPARK PLUG BLEW OUT ON THE PASSENGER SIDE OF MY 1999 MUSTANG GT WITH A 4.6...