NHTSA Complaint #10022541 — 1997 FORD GRAND MARQUIS
ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE issue reported to NHTSA
Complaint Details
| ODI Number | 10022541 |
| Vehicle | 1997 FORD GRAND MARQUIS |
| Component | ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | FL |
Consumer Description
1997 MERCURY GRAND MARQUIS CRACKED INTAKE MANIFOLD. *MR THE VEHICLE STALLED IN HEAVY TRAFFIC ALMOST HITTING AN 18 WHEELER AND FORD DENIED RESPONSIBILITY. THE WATER PUMP WAS REPLACED BUT THE STEAM CONTINUED TO ESCAPE AND THE PROBLEM WAS DIAGNOSED AS A CRACKED MANIFOLD. THE CONSUMER WAS TOLD THAT THIS WAS A WELL KNOWN PROBLEM FOR FORD BECAUSE THEY HAVE USED PLASTIC INTAKE FOR SOME TIME AND THE VEHICLES WERE SUBJECT TO HIGHER TEMPERATURES AND WOULD STOP IN TRAFFIC WITH NO WARNING. *SCC *JB
Related Complaints for the 1997 FORD GRAND MARQUIS
Other ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:MANIFOLD/HEADER/MUFFLER/TAIL PIPE Complaints
#10071446
WHILE DRIVING VEHICLE OVERHEATED DUE TO INTAKE MANIFOLD FAILURE. COOLANT LEAKED INTO THE ENGINE. DEALER NOTIFIED....
#10038018
WHEN DRIVING AT VARIOUS SPEEDS, THE INTAKE MANIFOLD CRACKED, WHICH CAUSED COOLANT TO LEAK OUT.*AK *JB
#10029884
CONSUMER STATES THERE IS A COOLANT SMELL COMING INTO THE CAB . ALSO HEAVY SMOKE COMIING FROM UNDER THE VEHICLE. DEAL...
#10029597
CONSUMER CALLED COMPLAINING ABOUT HAVING PROBLEMS WITH THE INTAKE MANIFOLD GASKET. MANIFACTURER WAS NOT CONTACTED AT ...
#10012509
THE VEHICLES INTAKE MANIFOLD CRACKED AND RESULTED IN COOLANT LEAK. *NLM *SCC
Recent Complaints for the 1997 FORD GRAND MARQUIS
#10091463
SERVICE BRAKES, HYDRAULIC:FOUNDATION COMPONENTS:HOSES, LINES/PIPING, AND FITTINGS
THE BRAKES PEDAL WENT TO THE FLOOR WHEN THEY WERE APPLIED. THE VEHICLE CONTINUED TO ACCELERATED IN SPEED. THE CONS...
#10071735
STRUCTURE:FRAME AND MEMBERS:UNDERBODY SHIELDS
WHEN THE BRAKES WERE APPLIED, THE VEHICLE PULLED TO THE RIGHT. THE VEHICLE WAS TAKEN TO SEARS AND THE TECHNICIAN DET...
#10048034
ENGINE AND ENGINE COOLING
WHILE DRIVING, THE TEMPERATURE GAUGE WAS VERY HIGH BECAUSE THE INTAKE MANIFOLD FAILED. THIS CAUSED THE COOLANT TO GO...
#10020346
ENGINE AND ENGINE COOLING:ENGINE
WHILE DRIVING, THE VEHICLE OVERHEATED. THE INTAKE MANIFOLD WAS REPLACED. *JB
#10017816
ELECTRICAL SYSTEM
THE VEHICLES FAULTY REGULATOR CAUSED PROBLEMS WITH THE POWER WINDOWS. *NLM