2007 DODGE MAGNUM Engine And Engine Cooling Problems

6 NHTSA complaints on file

Check any vehicle history by VIN - Free vehicle history report

Engine And Engine Cooling Issues in the 2007 DODGE MAGNUM

6 engine and engine cooling complaints have been filed with NHTSA for the 2007 DODGE MAGNUM. Of these, 0 involved a crash, 0 involved a fire, and 0 resulted in injury.

6
Complaints
0
Crashes
0
Fires
0
Injuries
0
Deaths

All Engine And Engine Cooling Complaints

#10622376 |
TL* THE CONTACT OWNS A 2007 DODGE MAGNUM. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 45 MPH, THE VEHICLE MADE A LOUD ABNORMAL NOISE. AFTER INSPECTING THE VEHICLE, THE CONTACT NOTICED THAT THE RADIATOR FAN HAD SEPARATED CAUSING DAMAGE TO THE RADIATOR. THE CONTACT REPLACED BOTH THE RADIATOR FAN AND RADIATOR. THE MANUFACTURER HAD BEEN NOTIFIED OF THE FAILURE. THE APPROXIMATELY FAILURE MILEAGE WAS 136,962. ..UPDATED 11/11/14*BF *BF UPDATED 12/02/14*JB
#10525773 |
FIRST INSTANCE, WHILE SLOWING DOWN FOR A STOP LIGHT FELT A SHUDDER AND ENGINE SHUT OFF, ALL OTHER SYSTEMS APPEARED NORMAL. COASTED TO STOP, ENGINE RESTARTED WITHOUT TROUBLE. NEAR FULL TANK OF FUEL. SECOND INSTANCE, WHILE IN A PARKING LOT SHIFTING FROM PARK TO REVERSE ENGINE SHUT OFF, ALL OTHER SYSTEMS APPEARED NORMAL AND ENGINE RESTARTED WITHOUT TROUBLE. FILLED FUEL TANK THE PREVIOUS DAY, 3/4 TANK TODAY. HAS HAPPENED ON OTHER OCCASIONS WHILE DRIVING AT SLOW SPEEDS BUT I DO NOT REMEMBER THE QUANTITY OF FUEL, EACH TIME THAT CAR HAS RESTARTED WITHOUT INSTANCE AND EACH TIME EVERYTHING ELSE APPEARED NORMAL. THE ENGINE ALWAYS SEEMS TO RUN PROPERLY AND ALL OF THE CARS OTHER SYSTEMS SEEM TO OPERATE NORMALLY. *TR
#10481153 |
CAR WOULD NOT SHIFT OUT OF PARK. PLASTIC RETAINER INSIDE THE SHIFTER ASSEMBLY WAS BROKEN. REMOVED SHIFTER ASSEMBLY AND DISASSEMBLED. REPLACED BROKEN PLASTIC PART WITH NEW METAL PART, REASSEMBLED AND REINSTALLED SHIFTER AND VERIFIED OPERATION. PARTS 11.79 MISC 13.86 LABOR 277.20 DODGE REFUSED ANY GOODWILL, SHOULD BE A RECALL DUE TO DEFECTIVE ORIGINAL PARTS BEING REPLACED WITH NEW AND IMPROVED PARTS. *TR THE CONSUMER STATED RECENTLY, THE CHECK ENGINE AND ETC LIGHTS ILLUMINATED. THE LOCAL DODGE DEALER CONSUMER THE CONSUMER THE VEHICLE A VERY LOW COMPRESSION IN CYLINDER #5 AND RECOMMENDED HAVING A VALVE JOB, AS WELL AS REPLACING THE WATER PUMP AND TIMING BELT, AT A COST OF $3,500. THE CONSUMER FOUND A LOCAL REPAIR SHOP THAT WAS WILLING TO DO THE WORK FOR $2,103. WHILE FIXING THE VEHICLE, IT WAS DISCOVERED THAT ONE OF THE VALVE GUIDES ON CYLINDER #5 HAD LET THE STEM RUN AT AN ANGLE...
#10424281 |
TL* THE CONTACT OWNS A 2007 DODGE MAGNUM RT. THE CONTACT WAS DRIVING 50 MPH WHEN THE VEHICLE OVERHEATED. THE VEHICLE WAS TAKEN TO THE DEALER WHO DIAGNOSED THAT THE COOLING FAN WAS FRACTURED AND HAD PUNCTURED THE RADIATOR. AS A RESULT, THE RADIATOR, FAN AND FAN MOTOR NEEDED TO BE REPLACED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE WHO DID NOT OFFER ANY ASSISTANCE SINCE THE VEHICLE WAS NOT INCLUDED IN ANY RECALLS. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 55,000.
#10420963 |
TL* THE CONTACT OWNS A 2007 DODGE MAGNUM. THE CONTACT STATED THE VEHICLE WOULD ROAR AND THEN DECELERATE WHEN ATTEMPTING TO ACCELERATE FROM A STOP. THE DEALER PERFORMED A SOFTWARE UPDATE HOWEVER, THE FAILURE PERSISTED. THE VEHICLE WAS TAKEN TO THE DEALER A SECOND TIME AND THE CONTACT WAS INFORMED THAT SHE NEEDED TO REPLACE THE ACTUATOR IDLE SENSOR AND THE UPPER INTAKE MANIFOLD. THE VEHICLE WAS ALSO TAKEN TO A PRIVATE MECHANIC WHO INFORMED THE CONTACT THAT THE VEHICLE WAS UNSAFE TO DRIVE. NO REPAIRS WERE PERFORMED. THE MANUFACTURER WAS AWARE OF THE FAILURE. THE CURRENT MILEAGE WAS 75,900. THE APPROXIMATE FAILURE MILEAGE WAS 35,000. UPDATED 01/03/12*LJ UPDATED 01/11/12
#10261598 |
2007 DODGE MAGNUM WHEN COMING TO A STOP OR IDLING ENGINE REVS UP AND GOES FORWARD A LITTLE. *TR
Check any vehicle history by VIN - Free vehicle history report