2007 DODGE DURANGO 4X4 Steering Problems

5 NHTSA complaints on file

Check any vehicle history by VIN - Free vehicle history report

Steering Issues in the 2007 DODGE DURANGO 4X4

5 steering complaints have been filed with NHTSA for the 2007 DODGE DURANGO 4X4. Of these, 0 involved a crash, 0 involved a fire, and 0 resulted in injury.

5
Complaints
0
Crashes
0
Fires
0
Injuries
0
Deaths

All Steering Complaints

#11223116 |
THE CRANKSHAFT POSITION SENSOR CONSISTENTLY GOING BAD , DUE TO FAULTY WIRING HARNESS OR OTHER ISSUES. THIS WILL CAUSE THE VEHICLE TO RANDOMLY SHUT OFF WHILE EITHER SITTING OR DRIVING , AND THE ITS UNKNOWN AS TO WHY IT IS HAPPENING. SUGGESTED REPAIR IS TO JUST REPLACE , BUT I REPLACE 1 A YEAR . I HAVE REPLACED 6 IN THE LAST 5 YEARS OF OWNING THIS VEHICLE. DEALERSHIP IS UNABLE TO LOCATE THE PROBLEM TO WHY THE CPS KEEPS FAILING .
#10614829 |
I BOUGHT THIS VEHICLE NEW IN 2007. I HAVE ONLY HAD MINOR PROBLEMS UNTIL THIS BEGAN. THE VEHICLE IDLE BEGAN FLUCTUATING WHILE SITTING STILL. IT WOULD REV TO 2000 RPMS AND DROP AND NEARLY STALL. IT DOESN'T HAPPEN REGULARLY, SO I WASN'T CONCERNED. THEN IT STALLED ON MY WIFE IN THE DRIVE THRU. I CLEANED THE THROTTLE BODY AND REPLACED ALL SPARK PLUGS AND COIL PACKS AT AROUND 60000. THIS HAD LITTLE OR NO EFFECT. WE CONTINUED TO DRIVE FOR A FEW MONTHS AND THEN THIS PROBLEM BEGAN. MY WIFE CALLED AND STATED IT LOST POWER STEERING AND THROTTLE, BUT THE ENGINE WAS STILL RUNNING. SHE TURNED IT OFF AND RESTARTED AND EVERYTHING WAS FINE. I THOUGHT SHE HAD MISTAKEN BECAUSE THE AC AND SOME GAUGES WILL OPERATE IF THE KEY IS ON BUT ENGINE IS OFF. THEN IT HAPPENED WHILE I WAS DRIVING. I WAS RUNNING 60 MPH AND...
#10503736 |
BROUGHT TRUCK IN FOR ENGINE LIGHT ON & NO POWER ON MARCH 9, 2013...CLAIMED SPARK PLUGS PUT IN BY MANUFACTURER WERE 30,000 MILES PLUGS....WHO DOES THAT ANYMORE. WHILE DOING THE TUNE UP, MECHANIC NOTICED FLUID DRIPPING. POWER STEERING PUMP WAS LEAKING. PUT NEW PUMP IN (MARCH 12, 2013) WHICH SEEMED TO BE BAD. ORDERED ANOTHER PUMP (ARRIVED MARCH 15, 2013) WHICH WORKED BUT THE RACK IN PINION STEERING BLEW SEALS ON BOTH ENDS. ORDERED PART WHICH TOOK SEVERAL DAYS TO COME IN (HOPEFULLY MARCH 20, 2013). THE MECHANIC BELIEVES THE RACK IN PINION WAS NOT RIGHT FROM THE BEGINNING. THIS WOULD ACCOUNT FOR THE FRONT TIRES WEARING QUICKLY & FUNNY. IT WOULD ALSO ACCOUNT FOR THE NOISE HEARD ON THE PASSENGER SIDE FRONT END WHEN HITTING BUMPS. BOTH THESE ISSUES WERE BROUGHT TO THE DEALERSHIPS ATTENTION PRIOR BUT NOTHING WAS DONE. CLAIMED THEY DIDN'T HEAR THE SOUND WHEN TEST DRIVING....
#10412310 |
TL* THE CONTACT OWNS A 2007 DODGE DURANGO 4X4. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 65 MPH, THE VEHICLE BEGAN TO SHAKE VIOLENTLY. THE CONTACT DROVE TO THE SIDE OF THE ROAD AND NOTICED THAT THE FRONT PASSENGER'S SIDE WHEEL WAS POINTNG OUTWARD, AWAY FROM THE VEHICLE. THE VEHICLE WAS TOWED TO AN AUTHORIZED DEALER WHO STATED THAT THE FAILURE WAS CONTRIBUTED TO A LOOSE TIE ROD. THE VEHICLE WAS IN THE PROCESS OF BEING REPAIRED. THERE WAS A RECALL POSSIBLY RELATED TO THE FAILURE UNDER NHTSA CAMPAIGN ID NUMBER 06V386000 (STEERING); AND THE CONTACT PLANNED TO NOTIFY THE DEALER TO VERIFY WHETHER THE VIN WAS INCLUDED. IN ADDITION, WHENEVER REFUELING, A SUBSTANTIAL AMOUNT OF FUEL WOULD SPRAY OUT OF THE FILLER NECK. THE MANUFACTURER WAS MADE AWARE OF THE FAILURES. THE APPROXIMATE FAILURE MILEAGE WAS 20,000. THE VIN WAS UNAVAILABLE.
#10340313 |
THE VEHICLE WAS OPERATING AT HIGHWAY SPEED WHEN THE RIGHT FRONT TIE ROD BROKE AT THE KNUCKLE. THERE WAS NO WARNING, ABNORMAL TIRE WEAR OR DAMAGE PRIOR TO THE FAILURE. THE VEHICLE WAS ON A EIGHT LANE HIGHWAY AND WAS ABLE TO GET OFF THE ROAD WITH OUT A CRASH. THE WHEEL SUSTAINED SUBSTANTIAL DAMAGE FROM THE LOOSE TIE ROD END. *TR
Check any vehicle history by VIN - Free vehicle history report