NHTSA Complaint #750030 — 1999 DODGE DURANGO
ENGINE AND ENGINE COOLING:ENGINE:GASOLINE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 750030 |
| Vehicle | 1999 DODGE DURANGO |
| Component | ENGINE AND ENGINE COOLING:ENGINE:GASOLINE |
| Date of Incident | |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | OH |
Consumer Description
VEHICLE BURNED EXCESSIVE OIL PRIOR TO ENGINE SEIZE AND WE WERE TOLD THIS WAS NORMAL BECAUSE OF THE VOLUME OF MILES TRAVELED ON THE VEHICLE. THIS WAS AFTER A ROUTINE OIL CHANGE AT KENWOOD DODGE. AS USUAL WE INQUIRED AS TO ANY FACTORY RECALLS. ON OUR WAY TO NEW HAMPSHIRE TO ATTEND THE FUNERAL FOR A RELATIVE, MY HUSBAND CHECKED THE OIL AS USUAL AND IT APPEARED TO BE FINE. NO OIL WAS ADDED AT THIS TIME. AFTER ENTERING NEW HAMPSHIRE IN THE TOWN OF PEMBROOKE, THE CHECK GAUGES LITE ILLUMINATED AND THEN THE OIL PRESSURE GAUGE DROPPED TO 0. WE IMMEDIATELY PULLED INTO A LOCAL AUTOZONE CAR CARE STORE AND MY HUSBAND THEN CHECKED THE OIL. THE DIPSTICK SHOWED APPROXIMATELY 1.5 QUARTS LOW AND SO AFTER SETTING FOR A SHORT WHILE OF ABOUT 35 MINUTES AND REPLENISHING THE OIL, WE PROCEEDED ON THE REST OF THE JOURNEY. AFTER TRAVELING APPROXIMATELY 20 OR SO MILES ON THE WINDING BACK ROADS MY HUSBAND NOTICED AN ERRATIC, LOUD KNOCKING SOUND COMING FROM THE ENGINE. HE THEN PULLED THE DURANGO TO THE SIDE OF THE ROAD WHEREBY THE KNOCKING WAS SO LOUD YOUR COULD NOT HEAR EACHOTHER TALK. HE THEN NOTICED THE OIL PRESSURE DROPPED AGAIN TO 0 AND IMMEDIATELY SHUT DOWN THE ENGINE. IT BANGED LOUDLY AT THIS POINT AS SMOKE SPEWED FROM THE RIGHT FRONT SIDE OF THE TRUCK. WE HAD THE DURANGO TOWED TO BONNEVILLE AND SONS DODGE IN MANCHESTER NH AND THE CONCURRED THE ENGINE HAD SEIZED. THEY HAD STATED THAT THE OIL AS WELL AS THE RADIATOR FLUID HAD LEAKED OUT AND THIS WAS UNTRUE AS WE HAD SEVERAL PEOPLE INSPECT THE TRUCK PRIOR TO THEIR DIAGNOSIS AND SAW NO EXTERNAL VIEWS OF ANY FLUID LEAKAGE. THE RADIATOR WAS FULL AND THE DIPSTICK WAS SEIZED IN THE ENGINE BLOCK. THE DEALER AS WELL AS DODGE SAID THIS WAS DUE TO LACK OF OIL CHANGES. THE OIL WAS CHANGED EVERY 5-7 THOUSAND MILES REGULARLY AND WAS ONLY THREE THOUSAND MILES PAST DUE FROM IT'S LAST CHANGE. I CAN'T IN MY WILDEST DREAMS IMMAGINE THIS IS THE RESULT OF OIL THAT WAS IN THE BLOCK AT THE TIME. WE DID FIND OUT HOWEVER THAT THIS IS COMMON.*AK
Related Complaints for the 1999 DODGE DURANGO
Other ENGINE AND ENGINE COOLING:ENGINE:GASOLINE Complaints
#10162409
COMPUTER CHIP FAILURE CAUSES VEHICLE TO SHUT DOWN. DEALER CONTACTED BUT WANTS TO CHARGE $1000 FOR AN EMISSIONS COVERE...
#10129469
DT: THE VEHICLE IS 1999 DODGE DURANGO. THE CONSUMER NEEDED THE TIRES REPLACED AND HE HAD AN INDEPENDENT MECHANIC CH...
#10117964
NO OIL PRESSURE, ENGINE SLUDGE, CLEANED. *AK
#10067833
BURNT VALVES AT 57,000. *AK
#10049788
I HAVE A 1999 DODGE DURANGO WITH 39000 AND THE BALL JOINTS ARE BAD. ALSO THE BRAKING SYSTEM SEEMS TO BE FAILING, IT G...
Recent Complaints for the 1999 DODGE DURANGO
#11463158
SERVICE BRAKES
Steel Brake lines burst. The Steel lines are all rusted and corroded. Even the factory replacement pieces corroded a...
#11362829
ELECTRICAL SYSTEM
PHANTOM MISFIRE CAN DROP ENGINE RPM AND STALL. EVERY POSSIBLE SENSOR REPLACED. FUEL PUMP, INJECTORS REPLACED. ENTIRE ...
#11362829
ENGINE
PHANTOM MISFIRE CAN DROP ENGINE RPM AND STALL. EVERY POSSIBLE SENSOR REPLACED. FUEL PUMP, INJECTORS REPLACED. ENTIRE ...
#11329114
POWER TRAIN
TL* THE CONTACT OWNS A 1999 DODGE DURANGO. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 5 MPH, THE VEHICLE ...
#11286786
ELECTRICAL SYSTEM
HELLO MY NAME IS [XXX] I BROUGHT THIS SUV 12/3/2019 .THE GUY I BOUGHT THIS SUV FROM HE TOLD ME THERE'S AN ELECTRICAL ...