NHTSA Complaint #11084704 — 2016 DODGE DURANGO
POWER TRAIN issue reported to NHTSA
Crash
Complaint Details
| ODI Number | 11084704 |
| Vehicle | 2016 DODGE DURANGO |
| Component | POWER TRAIN |
| Date of Incident | |
| Date Filed | |
| Mileage | 52,000 miles |
| Crash | Yes |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | MI |
Consumer Description
WHILE DRIVING THE VEHICLE A MESSAGE CAME UP ON THE CLUSTER "START/STOP SYSTEM DISABLED. SERVICE START/STOP SYSTEM". SHORTLY AFTER THERE WAS ANOTHER MESSAGE "LOW BATTERY MODE. SOME SYSTEMS FUNCTION REDUCED". I LOOKED AT THE SYSTEM HEALTH STATUS AND THE BATTERY VOLTAGE WAS AT 11.2 VOLTS. WHILE DRIVING THE VOLTAGE CONTINUED TO DROP. I CALLED THE DEALER AND THEY ASKED ME TO BRING THE VEHICLE IN TO CHECK DIAGNOSTICS. WHILE DRIVING TO THE DEALER THE VOLTAGE CONTINUED TO DROP AND THE RADIO TURNED OFF AND WOULD NOT TURN BACK ON. WHEN I ARRIVED AT THE DEALERSHIP THE VOLTAGE WAS AT ~10.1 VOLTS. WHEN I PULLED THE VEHICLE INTO THE DEALERSHIP SERVICE BAY THE SERVICE WRITER CAME OVER AND WE AGREED TO NOT SHUT OFF THE VEHICLE AS WE WEREN'T SURE WHETHER IT WOULD RESTART GIVEN THE BATTERY VOLTAGE. AS THE VEHICLE IDLED IN THE SERVICE BAY THE VOLTAGE CONTINUED TO DROP AND THE VOLTAGE WAS JUST OVER 9 VOLTS WHEN I GOT OUT OF THE VEHICLE. THE VEHICLE WAS RUNNING AND WAS IN PARK. PARKING BRAKE WAS NOT ENGAGED. A DEALERSHIP EMPLOYEE GOT INTO THE VEHICLE AND WAS GOING TO MOVE IT BUT THE SERVICE WRITER ASKED HIM TO LEAVE IT WHERE IT WAS UNTIL THEY DETERMINED WHICH TECHNICIAN IT WOULD BE ASSIGNED TO. THE DEALERSHIP EMPLOYEE TOLD ME THAT HE DID NOT MOVE THE VEHICLE AND DID NOT TAKE IT OUT OF PARK. I WENT INTO THE WAITING ROOM INSIDE THE DEALERSHIP AND A FEW MINUTES LATER THE SERVICE MANAGER CAME OUT TO TELL ME THAT THERE WAS AN ISSUE WITH MY VEHICLE AND THAT IT DROVE INTO A WALL IN THE SERVICE BAY WITH NO ONE IN THE VEHICLE. WHEN I WENT OUT INTO THE BAY THE RH FRONT WHEEL HAD CLIMBED A CURB AND THE VEHICLE HAD HIT A WALL. FCA SPECIAL INVESTIGATION TEAM REVIEWED VEHICLE AND DETERMINED THAT THERE WAS NO MECHANICAL ISSUE WHICH WOULD CAUSE THE VEHICLE TO MOVE ON ITS OWN. NO EXPLANATION WAS FOUND FOR LOW VOLTAGE CONDITION. DEALERSHIP HAS VIDEO OF INCIDENT.
Related Complaints for the 2016 DODGE DURANGO
Other POWER TRAIN Complaints
#11675495
Driving in the left lane of an interstate highway at 75mph, in moderate traffic, in daylight hours, clear weather, wi...
#11531768
WHILE MOVING THE CAR LOSES POWER, SHIFT TO P THEN DESIRED GEAR AND COMES TO A STOP. NOT ABLE TO STEER.
#11439842
The contact owns a 2016 Dodge Durango. The contact stated that his daughter was in the passenger seat when she activa...
#11433548
3 malfunctions within a month time frame. The car will start and run normally. Then it will suddenly come to a halt b...
#11429563
Very common cylinder 2 misfire. Replaced all spark plugs and the cylinder two ignition coil. Replaced upper and lower...
Recent Complaints for the 2016 DODGE DURANGO
#11697733
ELECTRICAL SYSTEM
We had an issue with an error message in the middle of driving that stopped the acceleration of the vehicle, this see...
#11692509
FUEL SYSTEM, GASOLINE
The contact owns a 2016 Dodge Durango. The contact stated that while driving at an undisclosed speed, there was a str...
#11677230
ELECTRICAL SYSTEM
The Rear License Plate Light bulb (right) was out and I went to have the bulb replaced. I was quoted over $1100 from...
#11677230
EXTERIOR LIGHTING
The Rear License Plate Light bulb (right) was out and I went to have the bulb replaced. I was quoted over $1100 from...