NHTSA Complaint #10765229 — 2009 BMW M3
ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10765229 |
| Vehicle | 2009 BMW M3 |
| Component | ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 56,729 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | TX |
Consumer Description
VEHICLE LOST POWER WHILE TAKING A TURN. I WAS ABLE TO RESTART IT AND DRIVE TO A NEARBY PARKING LOT. I DROVE AROUND SLOWLY TO TEST AND NOTICED KNOCKING NOISE FROM THE ENGINE. I ALSO NOTICED ENGINE TEMPERATURE WAS ABOVE NORMAL, NOT QUITE TO THE NEXT MARKER, BUT CLOSE. AT THAT POINT, I HAD THE CAR TOWED TO A BMW SERVICE SHOP. THEIR DIAGNOSIS WAS ROD BEARING FAILURE WHICH LED TO CRANKSHAFT DAMAGE, RESULTING IN AN ENGINE, WITH ONLY 57K MI, THAT IS NO LONGER REUSABLE. I AM NOW FACING ENGINE REPLACEMENT COSTS OF $15-25K.
Related Complaints for the 2009 BMW M3
Other ENGINE Complaints
#11002983
TAKATA RECALL DRIVING MY CAR FOR ABOUT 30 MINUTES ON THE LOCAL STREET AND STOPPED AT A RED LIGHT, LIGHT TURNS GREEN,...
#10917999
THE CAR SUDDENLY VIBRATED AND THE WHEELS LOCKED UP AND SKIDDED SLIGHTLY SIDEWAYS BEFORE GOING INTO A REDUCED POWER MO...
#10825875
S65 V8 ENGINE IN A BMW M3 E90/92/93 AND M5'S WITH A V10 HAS TWO THROTTLE VALVE ACTUATORS THAT FAIL PREMATURELY AT 40-...
Recent Complaints for the 2009 BMW M3
#11427001
ELECTRICAL SYSTEM: INSTRUMENT CLUSTER/PANEL
The contact owns a 2009 BMW M3. The contact stated while operating the vehicle, the driver’s and passenger’s side tur...
#11427001
EXTERIOR LIGHTING:HEADLIGHTS
The contact owns a 2009 BMW M3. The contact stated while operating the vehicle, the driver’s and passenger’s side tur...
#11318530
AIR BAGS
I RECEIVED A RECALL FOR THE AIRBAG ON MY CAR. I CONTACTED BMW TO REPLACE BUT THEY WERE UNABLE TO REPLACE AT THAT TIME...
#11060803
AIR BAGS
TAKATA RECALL - I HAVE BEEN WAITING 2 YEARS TO HAVE THIS RECALL DONE. I WAS ONCE SCHEDULED TO GET THE SERVICE AND THE...
#10991274
ELECTRICAL SYSTEM
VEHICLE WOULD NOT START AND ALL ELECTRICAL SYSTEMS WERE DEAD DESPITE A GOOD BATTERY. WAS SOLVED BY REMOVING GLOVE BO...