NHTSA Complaint #10626501 — 2014 NISSAN 370Z
POWER TRAIN issue reported to NHTSA
Complaint Details
| ODI Number | 10626501 |
| Vehicle | 2014 NISSAN 370Z |
| Component | POWER TRAIN |
| Date of Incident | |
| Date Filed | |
| Mileage | 2,970 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | CA |
Consumer Description
THIS INCIDENT OCCURRED AT A BUSY INTERSECTION DURING HEAVY TRAFFIC. MANUAL TRANSMISSION SUNNY, AIR TEMP APPROX 75 F. THE VEHICLE HAD BEEN DRIVEN APPOX 0.25 MILES & 2 MINUTES IMMEDIATELY PRIOR TO EVENT AND PARKED FOR THE PREVIOUS 4 HOURS. DRIVER PARTIALLY ENGAGED THE CLUTCH AND SHIFTED TO 1ST GEAR TO INITIATE FORWARD MOVEMENT OF THE VEHICLE FROM A COMPLETE STOP. AT A SPEED OF APPROX 10MPH THE DRIVER FULLY DEPRESSED THE CLUTCH PEDAL (TO DISENGAGE THE CLUTCH) TO COAST MOMENTARILY WITH TRAFFIC AND SHIFT TO 2ND GEAR. THE DRIVER PARTIALLY RE-ENGAGED THE CLUTCH WITH THROTTLE TO RESUME ACCELERATION WITH TRAFFIC. THE CLUTCH PEDAL FAILED TO RETURN TO THE FULLY ENGAGED, DEFAULT, POSITION DURING OPERATION; THE CLUTCH PEDAL RETURNED ONLY APPROXIMATELY 1/3 OF NOMINAL TRAVEL DISTANCE. CONCURRENTLY, THE CLUTCH DID NOT ENGAGE AND SLIPPED WITH REGULAR THROTTLE APPLIED FOR THE SHIFTING CONDITION. PUMPING OF THE CLUTCH PEDAL DID NOT RESTORE NORMAL CLUTCH PEDAL POSITION NOR NORMAL CLUTCH FUNCTION. FAILURE OF THE CLUTCH TO PROPERLY ENGAGE AND DISENGAGE PREVENTED THE DRIVER FROM FULLY AND SAFELY CONTROLLING THE VEHICLE. DRIVER FORCED TRANSMISSION TO NEUTRAL POSITION, INDICATED TO SURROUNDING TRAFFIC AND COASTED TO SHOULDER ACROSS MULTIPLE LANES. DRIVER NOTED THAT NO APPARENT OBSTRUCTION TO THE MECHANICAL OPERATION OF THE CLUTCH PEDAL WITHIN THE CABIN. DRIVER NOTED AN ODOR, PRESUMABLY FROM OVERHEATED CLUTCH OR HYDRAULIC FLUIDS. SUBSTANTIALLY NORMAL CLUTCH PEDAL AND CLUTCH FUNCTION RETURNED WITHIN SEVERAL MINUTES. THE VEHICLE WAS DRIVEN SEVERAL MILES AND PARKED FOR AN HOUR. NORMAL CLUTCH PEDAL AND CLUTCH FUNCTION WERE NOTED AFTER THIS HOUR. *TR
Related Complaints for the 2014 NISSAN 370Z
Other POWER TRAIN Complaints
#11683803
While driving my 2014 Nissan 370Z with only around 43,000 miles, the car suddenly made a loud bang in the rear area a...
#11329488
MY CLUTCH WOULD NOT COME OFF THE FLOORBOARD. I COULD NOT SHIFT INTO ANY GEAR. THIS HAPPEN 3 DIFFERENT TIMES AFTER I ...
#11228501
SUMMARY: THE VEHICLE CONCENTRIC SLAVE CYLINDER (CSC), A COMPONENT OF THE TRANSMISSION AND CLUTCH, FAILED ABRUPTLY ...
#11101448
AFTER DRIVING MY 2014 NISSAN 370Z FOR 40,000 MILES, THE CLUTCH STUCK TO THE FLOOR. I WAS AT AN INTERSECTION AND FINA...
#11092575
TL* THE CONTACT OWNS A 2014 NISSAN 370Z. WHILE DRIVING 20 MPH, THE CHECK ENGINE INDICATOR ILLUMINATED AND THE VEHICLE...
Recent Complaints for the 2014 NISSAN 370Z
#11683803
UNKNOWN OR OTHER
While driving my 2014 Nissan 370Z with only around 43,000 miles, the car suddenly made a loud bang in the rear area a...
#11683803
VEHICLE SPEED CONTROL
While driving my 2014 Nissan 370Z with only around 43,000 miles, the car suddenly made a loud bang in the rear area a...
#11413979
UNKNOWN OR OTHER
WHILE DRIVING VEHICLE ON HIGHWAY AND CITY STREET AT SPEEDS BETWEEN 45-65 MPH, PRESSURE WARNING LIGHT CAME ON. VEHICL...
#11394285
AIR BAGS
THE PASSENGER SIDE AIRBAG WILL NOT OPERATE WHEN THE PASSENGER IN THE VEHICLE IS LESS THAN 130 POUNDS. I HAVE SPOKEN ...
#11092575
ENGINE
TL* THE CONTACT OWNS A 2014 NISSAN 370Z. WHILE DRIVING 20 MPH, THE CHECK ENGINE INDICATOR ILLUMINATED AND THE VEHICLE...