NHTSA Complaint #10577323 — 2002 FORD F SERIES (HEAVY)
POWER TRAIN issue reported to NHTSA
Complaint Details
| ODI Number | 10577323 |
| Vehicle | 2002 FORD F SERIES (HEAVY) |
| Component | POWER TRAIN |
| Date of Incident | |
| Date Filed | |
| Mileage | 84,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | WA |
Consumer Description
ENGAGE CLUTCH PEDAL AND CLUTCH PEDAL WENT TO THE FLOOR. THEY HAVE A PLASTIC BUSHING THAT GOES AROUND A STEEL BALL FITTING TO HOLD CLUTCH CABLE TO CLUTCH PEDAL. IT IS SO BAD I CARRY EXTRA PLASTIC BUSHINGS WITH ME IN CASE OF FAILURE. MY CONCERN IS THAT WHEN I HAVE A FULLY LOADED TRUCK WITH CAMPER AND HORSE TRAILER IN TOE. I AM STUCK WITH A TRUCK STUCK IN GEAR AND NO WAY TO DISENGAGE CLUTCH. EVEN EMPTY THIS IS A SCARY UNCOMFORTABLE EXPERIENCE. THEY SHOULD HAVE A SOLID PIN FOR A CONNECTION NOT A CHEAP $5.00 PART THAT BREAKS EVERY 30,000 MILES. I HOPE THIS CAN BE CORRECTED BEFORE SOMEONE IS KILLED. *TR
Related Complaints for the 2002 FORD F SERIES (HEAVY)
Other POWER TRAIN Complaints
#10606185
ON 06/25/2014 I WAS DRIVING MY 2002 FORD F-250 SUPER DUTY 7.3 LITRE DIESEL SOUTH ON RT. 81 IN SYRACUSE NY. AT EXIT 81...
Recent Complaints for the 2002 FORD F SERIES (HEAVY)
#10606185
FUEL/PROPULSION SYSTEM
ON 06/25/2014 I WAS DRIVING MY 2002 FORD F-250 SUPER DUTY 7.3 LITRE DIESEL SOUTH ON RT. 81 IN SYRACUSE NY. AT EXIT 81...
#10389910
FUEL SYSTEM, GASOLINE
SPARK PLUG BLOW OUT. # 2 PLUG PASSENGER SIDE.THIS HAPPENED YESTERDAY MARCH 11,2011. MY TRUCK HAS 37,000 MILES ON IT....
#10132994
STEERING
THIS PROBLEM BEGAN WHEN THE TRUCK WAS PURCHASED NEW FROM THE DEALERSHIP. WE DIDN'T FIND OUT THE REAL PROBLEM UNTIL AB...