NHTSA Complaint #10547162 — 2002 FORD F SUPER DUTY
ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10547162 |
| Vehicle | 2002 FORD F SUPER DUTY |
| Component | ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 171,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | MT |
Consumer Description
SPARK PLUG EJECTED FROM HEAD, CAME OUT WITH SUCH FORCE AS TO BREAK THE COIL ON THE FUEL RAIL, SHATTER THE SPARK PLUG AND DISINTEGRATED THE SPARK PLUG BOOT. HAD TO TAP LARGER HOLE AND INSTALL THREADED INSERT SO A NEW SPARK PLUG COULD BE THREADED INTO HEAD AND TORQUED TO SPECS. REPLACED THE COIL AND BOOT AND REINSTALL THE FUEL RAIL AND INJECTORS TO MAKE THE TRUCK SERVICEABLE AGAIN. *TR
Related Complaints for the 2002 FORD F SUPER DUTY
Other ENGINE Complaints
Recent Complaints for the 2002 FORD F SUPER DUTY
#10904574
TIRES
SET OF 5 UNIROYAL LIBERATOR TIRES PURCHASED NEW, LT265-75-16 LOAD RANGE E, 2002 F-250 4X4 (OEM SIZE) *THESE TIRES...
#10731993
SERVICE BRAKES
MY 2002 F250 SUPERDUTY WITH 7.3L DIESEL WILL NOT TURN AT PARKING SPEEDS AND HIGHER SPEEDS IF APPLYING THE BRAKE. I H...
#10731993
STEERING
MY 2002 F250 SUPERDUTY WITH 7.3L DIESEL WILL NOT TURN AT PARKING SPEEDS AND HIGHER SPEEDS IF APPLYING THE BRAKE. I H...
#10670815
ELECTRICAL SYSTEM
THIS ACCELERATOR PEDAL WAS REPLACED BY FORD IN A FACTORY RECALL ON APRIL 2011. AT THE TIME THE ORIGINAL PEDAL WORKED...