NHTSA Complaint #10534232 β 2006 PONTIAC GRAND PRIX
ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10534232 |
| Vehicle | 2006 PONTIAC GRAND PRIX |
| Component | ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 72,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | OR |
Consumer Description
DRIVING ON THE INTERSTATE GOING ABOUT 65 MPG WHEN ALL OF A SUDDEN I LOST ALL ENGINE POWER AND THE ENGINE STALLED. CHECK ENGINE LIGHT CAME ON AND TRACTION CONTROL SYSTEM REMAINED ON. PULLED OVER AND SHUT OFF THE ENGINE. RESTARTED THE ENGINE, LIGHTS REMAINED ON AND WAS ONLY ABLE TO GO ABOUT 15 MPH. HAD TO DRIVE IT VERY CAREFULLY ABOUT 10 MILES INTO THE NEXT TOWN. NO SHOPS WERE OPEN AT THAT TIME OF NIGHT. HAD TO STAY THE NIGHT AND TOOK IT INTO A SHOP THE NEXT MORNING. ERROR CODE SAID THAT THE MASS AIR FLOW SENSOR WAS BAD. REPLACED AND DROVE IT AROUND FOR ABOUT 5 MILES. SEEMED TO BE RUNNING OK. DROVE NOT EVEN 60 MILES AND THE SAME THING HAPPENED AGAIN. TOOK IT INTO A SISTER REPAIR SHOP AND THEY REPLACED THE OTHER PART OF THE MASS AIR FLOW SENSOR. WAS ABLE TO DRIVE TO MY DESTINATION AND BACK WITH NO REAL ISSUES. HERE IT IS 7 MONTHS LATER AND DRIVING ON THE INTERSTATE AGAIN WHEN THE SAME ISSUE HAPPENS. CHECK ENGINE LIGHT CAME ON AND TRACTION CONTROL LIGHT CAME ON. WAS ABLE TO GET OFF THE SIDE OF THE ROAD BUT THIS TIME. I COULDN'T EVEN GET IT TO DRIVE 3 FEET. SAT ON THE SIDE OF THE INTERSTATE FOR 2 HOURS AT NIGHT WAITING FOR A TOW TRUCK TO COME GET ME. GOT IT INTO A SHOP THE NEXT MORNING AND SAME ISSUES. NEEDED A NEW MASS AIR FLOW SENSOR. REPLACE AND PICKED UP BUT THEN THE ENGINE STARTED GETTING REALLY HOT. WATCHED THE TRANSMISSION FLUID GO FROM 108 TO 258 DEGREES IN A MATTER OF MINUTES. PULLED OFF THE ROAD AND WATCHED THE FLUID BUBBLE OUT OF THE OVERFLOW. GOT THE ENGINE TO COOL DOWN A BIT. STARTED IT AND DROVE 4 MILES AND THE SAME CODES CAME UP AND THE ENGINE DID THE SAME THING. HAD THE CAR TOWED BACK TO THE SHOP AND WAS TOLD THAT THE COMPUTER NEEDED TO BE REPLACED. DID THAT AND IT NOW SURGES UPON START UP. THE SUPER CHARGER IS NOT REGISTERING AS BEING EITHER HOOKED UP OR WORKING NOW. I AM BEING TOLD THAT THERE ARE SEVERAL ISSUES THAT COULD BE CAUSING THIS. *TR
Related Complaints for the 2006 PONTIAC GRAND PRIX
Other ENGINE Complaints
#11482117
Seems like a bad motor gasket cause itβs a constant burning oil smell with no visible leaks at all
#11453149
Unknown
#11389713
MY CAR STARTED ON FIRE WHILE ON A CITY ROAD BECAUSE OF THE POWER STEERING PUMP PULLEY COMPLETELY SPRUNG OFF SERPENTIN...
#11364309
BAD ENGINE HAD WHILE DRIVING ALMOST CAUSED AN ACCIDENT BAD KNOCKING NOISE WITHIN THE MOTOR DO TO FAULTY PARTS MECHANI...
#11328988
TL* THE CONTACT OWNS A 2006 PONTIAC GRAND PRIX. THE CONTACT STATED THAT WHILE DRIVING VARIOUS SPEEDS, THE VEHICLE STA...
Recent Complaints for the 2006 PONTIAC GRAND PRIX
#11424356
AIR BAGS
got cutoff on a busy highway going 70mph and they slammed their brakes. i had 6 car lengths between us and immediatel...