NHTSA Complaint #10275521 — 2004 FORD F-150
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Fire
Complaint Details
| ODI Number | 10275521 |
| Vehicle | 2004 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 64,865 miles |
| Crash | No |
| Fire | Yes |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | WI |
Consumer Description
2004 F150 4.6LTR ENGINE. SPARK PLUG BLOW OUT #3 CYLINDER 64865 MILES. ORIGINAL FACTORY PARTS. SPOKE DIRECTLY TO FORD MOTORS THEY ACT AS IF THIS IS MY FAULT. THE PARTS HAVE NEVER BEEN CHANGED. FORD TOLD ME IT IS NOT COVERED UNDER WARRENTY BECAUSE THIS IS A MAINTANENCE PART. THE DEALER TOLD ME THAT THIS HAS BEEN A BIG PROBLEM FOR FORD. BUT THEY WONT HONOR TO FIX THE PROBLEM EVEN THOUGH IT IS A MECHANICAL FAILURE DUE TO BAD DESIGN. IT COST 600.00 TO FIX AND I BELEIVE THIS SHOULD BE COVERED BY FORD DUE TO THE NUMBER OF INSTENCES. THERE WERE TWO TRUCKS FIXED THE SAME DAY FOR THE SAME PROBLEM AND AGAIN THE SERVICE DEPARTMENT SAID THIS HAS BEEN A BIG ISSUE. I WOULD LIKE THIS TO BE RESOLVED. THE CONSUMER SHOULD NOT HAVE TO WORRIE ABOUT A SPARK PLUG BLOWING OUT WHILE DRIVING. THIS IS A SAFTEY ISSUE BECAUSE FUEL KEEPS FLOWING INTO THE CYLINDER AND WHEN IGNIGHTS FLAMES FLY OUT THROUGH THE SPARK PLUG HOLE. QUIT ACTING LIKE TH IS IS NOT A PROBLEM AND RECALL THESE POOR DESINGED PARTS BEFORE SOMEONE DOES GET HURT. *TR
Related Complaints for the 2004 FORD F-150
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10412416
TL* THE CONTACT OWNS A 2004 FORD F150. WHILE DRIVING 40 MPH, THE CONTACT STATED THAT THE VEHICLE BEGAN TO SHAKE EXCE...
#10409728
S10 APPROPRIATE HANDLING- LETTER FROM DOJ FORWARDING A LETTER FROM RE HIS 2004 FORD F-150 *TGW THE CONSUMER STATED T...
#10402865
TL*THE CONTACT OWNS A 2004 FORD F150. THE CONTACT STATED DURING ROUTINE MAINTENANCE WITH A LOCAL MECHANIC HE WAS ADVI...
#10382993
TL* THE CONTACT OWNS A 2004 FORD F-150. THE CONTACT WAS DRIVING 10 MPH AS THE VEHICLE BEGAN JERKING VIOLENTLY. THE MA...
#10370827
THE #3 SPARK PLUG WAS EJECTED FROM THE ENGINE BLOCK. UPON INSPECTION, THE THREADS WERE STRIPPED AND DAMAGED BEYOND B...