NHTSA Complaint #10247144 — 2004 FORD F-150
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10247144 |
| Vehicle | 2004 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 41,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | FL |
Consumer Description
FORD MOTOR COMPANY HAS DESIGNED A DEFECTIVE HEAD DESIGN THAT CAUSES SPARK PLUGS TO GET STUCK IN THE HEAD WHEN SERVICE IS ATTEMPTED. THE 100K MILE INTERVAL IS TOO LONG, EVEN SUB 50K MILES IS UNACCEPTABLE. THE CARBON BUILDUP AROUND THE LONG 2 PIECE SPARK PLUG CAUSES THE LOWER, CRIMPED ON PART TO STAY IN THE HEAD WHILE THE TOP 2/3 AND ELECTRODE COME OUT WHEN CHANGING THE PLUG. THIS DESIGN HAS BEEN PUT IN USE FOR 4 YEARS ON ALL 5.4L 3VALVE MOTORS. FORD HAS A TSB THAT ACKNOWLEDGES THE PROBLEM, BUT THEIR REMEDY STILL DOES NOT HELP. ONCE THE PLUGS, BROKEN AND UNBROKEN, ARE REMOVED, PUTTING NICKEL ANTI-SEIZE ON THE THREADS STILL DOES NOT REMEDY THE ISSUE BECAUSE THE THREADS ON THE PLUG ARE NOT WHAT IS STICKING. THE LOWER PART OF THE SPARK PLUG IS WHAT CAUSES THE TROUBLE. FORD HAS EVEN DESIGNED A TOOL TO REMOVE THE OFTEN BROKEN PLUGS. THIS JUST RIDICULOUS AND A SOLUTION NEEDS TO BE MADE BEFORE A VERY LARGE CLASS ACTION SUIT IS DRAWN UPON FOMOCO. *TR
Related Complaints for the 2004 FORD F-150
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10412416
TL* THE CONTACT OWNS A 2004 FORD F150. WHILE DRIVING 40 MPH, THE CONTACT STATED THAT THE VEHICLE BEGAN TO SHAKE EXCE...
#10409728
S10 APPROPRIATE HANDLING- LETTER FROM DOJ FORWARDING A LETTER FROM RE HIS 2004 FORD F-150 *TGW THE CONSUMER STATED T...
#10402865
TL*THE CONTACT OWNS A 2004 FORD F150. THE CONTACT STATED DURING ROUTINE MAINTENANCE WITH A LOCAL MECHANIC HE WAS ADVI...
#10382993
TL* THE CONTACT OWNS A 2004 FORD F-150. THE CONTACT WAS DRIVING 10 MPH AS THE VEHICLE BEGAN JERKING VIOLENTLY. THE MA...
#10370827
THE #3 SPARK PLUG WAS EJECTED FROM THE ENGINE BLOCK. UPON INSPECTION, THE THREADS WERE STRIPPED AND DAMAGED BEYOND B...