NHTSA Complaint #10237816 — 2001 FORD TAURUS
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10237816 |
| Vehicle | 2001 FORD TAURUS |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 96,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | UT |
Consumer Description
TL*THE CONTACT OWNS A 2001 FORD TAURUS. WHILE DRIVING 30-40 MPH, THE VEHICLE WOULD SUDDENLY SHUT OFF LOSE POWER STEERING ABILITY. THE VEHICLE WOULD DRIFT TO A STOP AND THE INTERIOR LIGHTS REMAINED ILLUMINATED ON THE INSTRUMENT PANEL. DURING THE FIRST FEW FAILURES, THE CONTACT WAS ABLE TO PULL THE VEHICLE TO THE SIDE OF THE ROAD AND WALK HOME. SHE SENT HER HUSBAND TO CHECK THE VEHICLE AND IT STARTED UP NORMALLY. ON OTHER OCCASIONS, IT WOULD TAKE HOURS TO DAYS BEFORE THE VEHICLE COULD BE RESTARTED. TWO DIFFERENT MECHANICS HAVE PERFORMED DIAGNOSTIC TESTS ON THE VEHICLE AND THEY BOTH STATED THAT THE CAUSE OF THE FAILURE WAS THE BOX INSTALLED ON THE VEHICLE BY THE LOAN COMPANY. THE CONTACT CALLED THE LOAN COMPANY AND THEY INFORMED HER TO CALL THEIR TECHNICIAN. THE TECHNICIAN STATED THAT IT WAS NOT THE BOX, EVEN THOUGH IT HAD NOT YET BEEN INSPECTED. HE ALSO REFUSED TO REPLACE THE BOX UNLESS THE CONTACT PAID $80 FOR THE INSPECTION SERVICE. THE FAILURE MILEAGE WAS 96,000 AND CURRENT MILEAGE WAS 96,500.
Related Complaints for the 2001 FORD TAURUS
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10328807
MY 2001 FORD TAURUS ENGINE STOPS WORKING AFTER DRIVING FOR A WHILE. ON SEVERAL OCCASIONS IT STOPPED WHILE DRIVING ON ...
#10325616
REAR COIL SPRINGS AND HEAD GASKET I DIDN'T KNOW HOW TO DESCRIBE THE HEAD GASKET FROM THE CHOICES. *TR
#10200206
TL*THE CONTACT OWNS A 2001 FORD TAURUS. WHEN THE AIR CONDITIONER WAS TURNED ON, THE ENGINE WOULD STALL. THE WEATHE...
#10138088
DT: CONTACT OWNS A 2001 FORD TAURUS. THE CONTACT STATED WHILE DRIVING AT ANY SPEED VEHICLE STALLED. THE CONTACT STA...
#10124929
DT: WITHOUT WARNING THE HEAD GASKET BLEW OUT. WHILE DRIVING CALLER LOST POWER AND HAD TO PULL OFF THE SIDE OF ROAD....