NHTSA Complaint #10235626 — 2002 FORD F-250 SD
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Complaint Details
| ODI Number | 10235626 |
| Vehicle | 2002 FORD F-250 SD |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 91,573 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | MI |
Consumer Description
2002 FORD F250 CREW CAB 4X4 SHORT BOX, 5.4L V-8 GASOLINE ENGINE JUST UNDER 92000 MILES. ON 7/21/2008 MERGING ON THE EXPRESSWAY UNDER HEAVY ACCELERATION, A LOUD BANG WITH SPRING POPPING SOUND WAS HEARD FROM THE ENGINE FOLLOWED BY THE DISTINCT ODOR OF EXHAUST AND UNBURNED GASOLINE. VERIFIED THROTTLE CONTROL AND CONTINUED TO DRIVE WITH LOUD NOISE COMING FROM ENGINE. DROVE 4 MILES TO WORK TO SAFELY INSPECT THE PROBLEM. NOTED THAT THE EXHAUST Y-PIPE WAS SEPARATED FROM THE DRIVERS SIDE EXHAUST MANIFOLD. ASSUMING THAT IT WAS JUST A FAILED MANIFOLD BOLT, DROVE ~20 MILES TO THE DEALERSHIP TO HAVE IT LOOKED AT. RECEIVED THE CALL THAT THE NUMBER 6 SPARK PLUG WAS EJECTED FROM THE HEAD. UPON THE DEALERSHIPS INSPECTION, FOUND THAT THE THREADS WERE STRIPPED OUT OF THE HEAD. THE SPARK PLUG THEN ARRESTED IN THE IGNITION COIL WHICH WAS SEPARATED FROM THE HEAD DUE TO FAILURE OF ITS MOUNTING FLANGE. THE IGNITION WIRE HELD THE COIL AND PLUG ON THE ENGINE. THERE WAS ZERO GAP NOTED ON THE SPARK PLUG ELECTRODE WITH ANTI-SEIZE COMPOUND ON ONLY ABOUT .5" OF THE SPARK PLUG THREAD. THUS SUGGESTED THAT ONLY .5" OF THREAD ENGAGEMENT WAS PRESENT FROM THE FACTORY ORIGINAL PLUGS (I.E. THE SPARK PLUGS WERE NOT REPLACED SINCE THE RECOMMENDED REPLACEMENT INTERVAL IS 10 YEARS 100000 MILES). ADVISED THAT AT A MINIMUM A HEAD NEEDED TO BE REPLACED, BUT THAT AN ENGINE MAY BE A BETTER ECONOMICAL CHOICE SO THAT BOTH HEADS ARE REPLACED AND THIS DESIGN ISSUE COULD BE OVERCOME (THE NEWLY REMANUFACTURED ENGINE IS SUPPOSED TO HAVE LARGER THREAD ENGAGEMENT AT APPROXIMATELY .75"). ENGINE REPLACED TO INSURE THAT THIS FAILURE WOULD NOT OCCUR ON ONE OF THE OTHER CYLINDERS IN THE HEAD THAT WOULD NOT BE REPLACED. *TR
Related Complaints for the 2002 FORD F-250 SD
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10429430
SPARK PLUG IN THE #8 CYLINDER WAS BLOWN OUT BREAKING THE COIL PACK AND MESSING THE THREADS UP INSIDE THE HEAD ON THE ...
#10335960
LEAKING HEAD GASKETS ON 2002 FORD F250 TRUCK WITH 5.4L ENGINE ALLOWS OIL TO LEAK ONTO STARTER AND EXHAUST MANIFOLD CR...
#10321664
I HAD A SPARK PLUG BLOW OUT OF MY CYLINDER HEAD OF MY FORD F250 2002 WITH 79,000 MILES ON IT.
#10319012
I HAVE A 2002 FORD F250 WITH A TRITON V* ENGINE. TO THIS DATE, IT HAS BLOWN OUT 5 SPARK PLUGS! SO FAR, THE REPAIRS ...
#10311728
I OWN A 2002 F250 V10 WITH APPROX 84,000 MILES. I WAS JUST DRIVING ALONG AND THE SPARK PLUG FROM THE # 8 CYLINDER BL...
Recent Complaints for the 2002 FORD F-250 SD
#10981538
ELECTRICAL SYSTEM
MY SPEED CONTROL STOPPED WORKING IN 2012. IT IS A FORD F-250 SUPER DUTY. VIN [XXX]. INFORMATION REDACTED PURSUA...
#10981538
VEHICLE SPEED CONTROL
MY SPEED CONTROL STOPPED WORKING IN 2012. IT IS A FORD F-250 SUPER DUTY. VIN [XXX]. INFORMATION REDACTED PURSUA...
#10969530
SEAT BELTS
THE SEAT BELTS COME UNBUCKLED WHEN DRIVING. THIS HAPPENS TO THE DRIVE'S SIDE MORE OFTEN THAN PASSENGER SIDE. THE BELT...
#10945677
ENGINE
TRUCK DIES WHILE DRIVING WITHOUT ANY WARNING, CAN-NOT FIND THE PROBLEM AND FORD WILL NOT ACKNOWLEDGE THAT THERE IS AN...
#10861904
UNKNOWN OR OTHER
AFTER DRIVING ABOUT 30 MILES AND RETURNING HOME, THE TRUCK CAUGHT FIRE WHILE SITTING IN THE DRIVEWAY - ABOUT 20 MINUT...