NHTSA Complaint #10213228 — 1998 LEXUS GS
SUSPENSION:FRONT:CONTROL ARM:LOWER BALL JOINT issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10213228 |
| Vehicle | 1998 LEXUS GS |
| Component | SUSPENSION:FRONT:CONTROL ARM:LOWER BALL JOINT |
| Date of Incident | |
| Date Filed | |
| Mileage | 192,640 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | CA |
Consumer Description
ANOTHER LEXUS GS-300 OWNER FILED THIS REPORT ON MARCH 6, 2007: "WE OWN A 1998 LEXUS, MODEL GS 300. THIS SATURDAY MY WIFE WAS DRIVING THE LEXUS AND THE ENTIRE WHEEL ASSEMBLY CAME OFF THE VEHICLE DUE THE FAILURE OF THE LOWER BALL JOINT. IN REVIEWING RECALL INFORMATION FOR LEXUS\TOYOTA, IT IS VERY APPARENT THERE IS AN ONGOING ISSUE OF QUALITY CONTROL RELATED TO THEIR LOWER BALL JOINTS. FOR OUR SPECIFIC MODEL, THERE WAS A RECALL IN 93, 94, 95, 96 AND 97 SPECIFIC TO THIS PART. GIVEN WE HAVE A 98 AND A RECALL HAS NOT BEEN ISSUED (YET), THE LEXUS DEALERSHIP REFUSED TO PROVIDE US WITH ANY ACCOMMODATION TOWARDS FIXING THE FAILED PART, OR THE RESULTING BODY DAMAGE RELATED TO THE VEHICLE TRAVELING DOWN THE ROAD ON ONLY THREE WHEEL. FORTUNATELY, WE WERE NOT TRAVELING ON THE HIGHWAY, BUT A SIDE STREET WHEN THIS INCIDENT OCCURRED. BUT MOREOVER, REGARDLESS OF OUR FINANCIAL LOSS, IN MY OPINION, THIS IS A PUBLIC SAFETY CONCERN..." WE EXPERIENCED A SIMILAR FAILURE WHEREIN THE LOWER DRIVER'S SIDE BALL JOINT FAILED WHILE BACKING OUT OF OUR DRIVEWAY. PRIOR TO THIS EVENT THE WHOLE FRONT SUSPENSION HAS BEEN MAKING A "CREAKING" NOISE DURING SLOW DRIVING WHILE TURNING. *TR
Related Complaints for the 1998 LEXUS GS
Recent Complaints for the 1998 LEXUS GS
#11476619
POWER TRAIN
On July 29th at approximately 8:30pm, I got into my car after exiting the Meijer store and noticed the car making str...
#11476619
SERVICE BRAKES
On July 29th at approximately 8:30pm, I got into my car after exiting the Meijer store and noticed the car making str...
#11476619
VEHICLE SPEED CONTROL
On July 29th at approximately 8:30pm, I got into my car after exiting the Meijer store and noticed the car making str...