NHTSA Complaint #10188616 — 2006 PONTIAC GTO
SUSPENSION issue reported to NHTSA
Complaint Details
| ODI Number | 10188616 |
| Vehicle | 2006 PONTIAC GTO |
| Component | SUSPENSION |
| Date of Incident | |
| Date Filed | |
| Mileage | 3,186 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | NJ |
Consumer Description
2006 PONTIAC GTO BLOWN RIGHT-FRONT STRUT (AT APPROX. 3180 MILES) FLATBED TOWED TO DEALERSHIP BURNS PONTIAC -GMC TRUCK, INC. 500 W RTE 70 MARLTON, NJ 08053 PHONE: 856-983-6060 FAX: 856-983-4770. *TR
Related Complaints for the 2006 PONTIAC GTO
Other SUSPENSION Complaints
#10660176
I HAVE A 2006 GTO THAT WAS MAKING A LOUD HUMMING NOISE BETWEEN 20 AND 50 MPH AFTER A 5,600 MILE ROAD TRIP WHICH TURNE...
#10425143
MY TIRES ON MY 2006 GTO ARE WEARING ON THE INSIDE OF THE TIRE AND BLOWING OUT MY TIRE IT APPEARS TO BE RUBBING ON THE...
#10375298
I WISH TO KNOW WHY NHTSA DID NOT HAVE A RECALL OF PONTIAC GTO'S FOR THE YEARS 2004, 2005, AND 2006..WHEN 200+ COMPLAI...
#10350662
HELLO, I WOULD LIKE TO SEND YOU A COMPLAINT CONCERNING THE SAFETY OF MY VEHICLE. I OWN A 2006 PONTIAC GTO. MY CAR CUR...
#10323724
I HAVE A 2006 PONTIAC GTO WITH JUST OVER 14,000 MILES ON THE ODOMETER. I WAS GETTING AN OIL CHANGE DONE AND THE CAR ...
Recent Complaints for the 2006 PONTIAC GTO
#10863248
POWER TRAIN
MY 2006 PONTIAC CABLE SHIFTER WAS INSPECTED SOME TIME ON NOVEMBER 2014! PROBLEM IS THE CABLE SHIFTER ON MAY 1 2016! T...
#10733609
POWER TRAIN:CLUTCH ASSEMBLY
TL* THE CONTACT OWNS A 2006 PONTIAC GTO. WHILE PARKED, THE VEHICLE FAILED TO SHIFT FROM THE NEUTRAL POSITION. THE VEH...
#10670426
POWER TRAIN
TL* THE CONTACT OWNS A 2006 PONTIAC GTO. THE CONTACT STATED THAT THE CLUTCH PEDAL BECAME LOOSE AND THE TRANSMISSION F...
#10670426
POWER TRAIN:CLUTCH ASSEMBLY:PEDAL/HAND LEVER(MOTORCYCLE)
TL* THE CONTACT OWNS A 2006 PONTIAC GTO. THE CONTACT STATED THAT THE CLUTCH PEDAL BECAME LOOSE AND THE TRANSMISSION F...
#10620941
ELECTRICAL SYSTEM
TL* THE CONTACT OWNS A 2006 PONTIAC GTO. THE CONTACT STATED THAT THE KEY BECAME STUCK IN THE IGNITION AND WAS UNABLE ...