NHTSA Complaint #10186743 — 1997 ACURA INTEGRA
AIR BAGS issue reported to NHTSA
Crash 1 Injury Vehicle Towed
Complaint Details
| ODI Number | 10186743 |
| Vehicle | 1997 ACURA INTEGRA |
| Component | AIR BAGS |
| Date of Incident | |
| Date Filed | |
| Mileage | 11,300 miles |
| Crash | Yes |
| Fire | No |
| Injuries | 1 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | FL |
Consumer Description
TL*- THE CONTACT'S SON WAS DRIVING THE 1997 ACURA INTEGRA IN THE EVENING HOURS GOING AROUND THE OFF RAMP OF THE EXPRESSWAY. THE DRIVER STATED THAT THE STEERING WHEEL LOCKED AND HE WAS NOT ABLE TO CONTROL, AND THE VEHICLE AND HIT AN EMBANKMENT OFF THE EXPRESSWAY. THE CONTACT WAS CONCERNED THAT THE AIR BAGS DIDN'T DEPLOY. THE VEHICLE WAS TRAVELING AT 25 MPH WHICH WAS THE SPEED LIMIT, AND THAT IT HAD DRIZZLED. HE FELT THAT THE AIR BAGS SHOULD HAVE DEPLOYED, AND IT WOULD HAVE SAVED THE DRIVER FROM SOME OF THE INJURIES THAT HE SUSTAINED. THE DRIVER HAD NECK, LOWER BACK AND HEAD INJURIES. THE CONTACT WILL SUBMIT PICTURES ALONG WITH POLICE AND INSURANCE COMPANY REPORTS. THE CONTACT STATED THAT THE POLICE OFFICER STATED THAT THE LOW PROFILE TIRES WERE WORN OUT ON THE INSIDE, BUT THE TIRES WERE ABOUT THREE MONTHS. THE FAILURE MILEAGE WAS 11,300.*AK
Related Complaints for the 1997 ACURA INTEGRA
Recent Complaints for the 1997 ACURA INTEGRA
#10947980
ELECTRICAL SYSTEM
I AM A 78 YEAR OLD WOMAN DEALING WITH MALES AT ACURA/HONDA WHO HAVE DONE NOTHING BUT RUN AROUND AND STALL. I HAVE HAD...
#10947980
ENGINE
I AM A 78 YEAR OLD WOMAN DEALING WITH MALES AT ACURA/HONDA WHO HAVE DONE NOTHING BUT RUN AROUND AND STALL. I HAVE HAD...
#10947980
VEHICLE SPEED CONTROL
I AM A 78 YEAR OLD WOMAN DEALING WITH MALES AT ACURA/HONDA WHO HAVE DONE NOTHING BUT RUN AROUND AND STALL. I HAVE HAD...
#10419500
ELECTRICAL SYSTEM
TL* THE CONTACT OWNS A 1997 ACURA INTEGRA. THE CONTACT STATED THAT THE SPEEDOMETER WAS INOPERATIVE. THE DEALER WAS C...
#10297400
ELECTRICAL SYSTEM
CAR WAS PARKED FOR ABOUT 4 HOURS. STARTED CAR AND IT STARTED TO OVERHEAT AND MAKE NOISE SO IGNITION KEY WAS TURNED O...