NHTSA Complaint #10183862 — 2006 FORD FOCUS
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10183862 |
| Vehicle | 2006 FORD FOCUS |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 4,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | UT |
Consumer Description
I'VE HAD MY 2006 FOCUS ST FOR ABOUT A YEAR NOW. SINCE I BOUGHT MY CAR I HAVE HAD TO HAVE 3 DIFFERENT ENGINES PUT IN IT. THE ORIGINAL MOTOR THREW A PISTON ROD DOWN THE BOTTOM OF MY ENGINE AND OUT. THEY SAID IT WAS POOR CASTING ON THE CRANKSHAFT. THIS WAS AT ABOUT 4,000 MILES. THEN AT ABOUT 15,000 MILES IT DID THE SAME THING ONLY THIS TIME I CAUGHT IT BEFORE IT BLEW. NEEDLESS TO SAY I HAD TO HAVE A NEW ENGINE ...AGAIN. WHAT HAPPENED IS MY ROD BEARINGS WENT OUT WHICH IS MOST LIKELY WHAT HAPPENED THE FIRST TIME, CAUSING MY ENGINE TO COMPLETELY THROW A PISTON ROD. NOW I AM ON MY 3RD ENGINE AND HOPING THAT THIS ONE STICKS. THE MECHANICS ARE VERY PUZZLED WHY THIS IS HAPPENING. THEY HAVE RUN ALL THE DIAGNOSTICS TO PROVE I HAVEN'T BEEN RACING AND I GET REGULAR OIL CHANGES THROUGH THE DEALERSHIP. FORD IS TRYING TO GET TO THE BOTTOM OF IT. GOOD NEWS IS 2 MORE TIMES IT'S A LEMON. BAD NEWS IS I HAVE HAD TO DEAL WITH MISSED TIME AT WORK AND THE INCONVENIENCE OF IT ALL. BEWARE BUT, THIS DOESN'T SEEM TO BE A REGULAR OCCURRENCE AMONG FOCUS OWNERS. *JB
Related Complaints for the 2006 FORD FOCUS
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10253123
2006 FOR FOCUS 2.0 I-4 BLEW OUT SPARK PLUG OUT OF THE HEAD N WITH IGNITION COIL. END RESULT FINDING THAT THE CAR HAD ...
Recent Complaints for the 2006 FORD FOCUS
#11546095
POWER TRAIN
Driving on hiway and vehicle shifted gears. Would no shift normally afterwards. Tried several times. Left myself and...
#11546095
UNKNOWN OR OTHER
Driving on hiway and vehicle shifted gears. Would no shift normally afterwards. Tried several times. Left myself and...
#11534659
UNKNOWN OR OTHER
Shifting linkage, was driving and went to shift into next gear and nothing. Clutch engaged, shifter goes in slot but ...
#11504620
SUSPENSION
The welded retainer of the front bushing on the right side lower (control) arm had rusted through. This allowed the ...
#11363545
ELECTRICAL SYSTEM
THE WIRING HARNESS FLEXES WHERE IT PASSES FROM THE BODY TO THE TAILGATE CAUSING THE IINSULATION AND WIRING TO BREAK A...