NHTSA Complaint #10171390 — 1999 FORD F-150

ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA

Check any vehicle history by VIN - Free vehicle history report
Vehicle Towed

Complaint Details

ODI Number 10171390
Vehicle 1999 FORD F-150
Component ENGINE AND ENGINE COOLING:ENGINE
Date of Incident
Date Filed
Mileage 81,791 miles
Crash No
Fire No
Injuries 0
Deaths 0
Vehicle Towed Yes
State OH

Consumer Description

I PURCHASED MY '99 FORD F-150 IN THE SPRING OF '04. AT THE TIME OF PURCHASE THE TRUCK HAD JUST OVER 49,000 MILES ON IT. THIS PAST MONDAY (10/16/06) WHILE PULLING OUT OF A LOCAL PARKING LOT, THE #2 SPARK PLUG WAS EJECTED OUT OF THE RIGHT CYLINDER HEAD, RIPPING OUT THE THREADS THAT THE SPARK PLUG SCREWS INTO & DESTROYING THE COIL PACK LOCATED DIRECTLY ABOVE. MY TRUCK ON THE DAY OF FAILURE HAD 81,790 MILES ON IT. THAT'S 18,210 MILES SHORT IF THE TRUCKS FIRST MANUFACTURES SUGGESTED 100,000 MILE TUNE-UP. FORD WILL NOT EVEN CONSIDER THE THOUGHT OF MAKING THIS MANUFACTURER'S DEFECT RIGHT. THEY SIMPLY TOLD ME THAT THE HEAD WOULD NEED TO BE REPLACED AT MY EXPENSE AND AT THE COST OF $2,800.00 TO $3,000.00. IT'S A DESIGN FLAW!!! THE ALUMINUM HEADS FOR THE 5.4 L ENGINES WERE ENGINEERED WITH AN INADEQUATE NUMBER OF THREADS NEEDED TO RETAIN THE SPARK PLUGS. THERE ARE ONLY 4 TO 5 THREADS TAPPED INTO THESE HEADS (APPROX. 1/4" TO 5/16" IN LENGTH) TODAY IS OCTOBER 19TH AND I HAVE PURCHASED A REPAIR KIT MANUFACTURED BY DORMAN PRODUCTS TO FIX THIS STRIPPED OUT SPARK PLUG MYSELF. THIS KIT IS SPECIFICALLY MADE BY DORMAN NOT FORD, TO FIX THIS PROBLEM OF FORDS 5.4L ENGINES. IT'S REALLY SAD THAT FORD HAS TO USE THE CONSUMERS AS GUINEA PIGS AND THEN FAIL SO MISERABLY TO BACK THEIR PRODUCT. I'M HESITANT TO CHECK THE TORQUE OF THE OTHER SEVEN PLUGS IN FEAR THAT THEY WILL NOT WITHSTAND THE RECOMMENDED 25 FOOT POUNDS OF TORQUE REQUIRED TO TIGHTEN THEM UP BUT IF I DON'T THEN IT'S RUSSIA ROULETTE AS TO WHEN THE NEXT ONE WILL BLOW OUT AND WHERE I WILL BE STRANDED WHEN IT DOES. I EXPECT FORD TO STAND BEHIND THEIR PRODUCT 110%, ESPECIALLY WHEN IT IS A WELL KNOWN FACT BY FORD AND THE CONSUMER THAT THERE IS AN ENGINEERING FLAW WITH THE DESIGN OF THE 5.4L ENGINES ALUMINUM HEADS PRODUCED BETWEEN YEARS OF 1997 THROUGH 2002. *NM

Related Complaints for the 1999 FORD F-150

Other ENGINE AND ENGINE COOLING:ENGINE Complaints

#10392544 WHILE DRIVING 45MPH ON SUBURBAN TWO LANE HIGHWAY I HEARD A LOUD BANG AND SUBSEQUENT RHYTHMIC POPPING SOUND ACCOMPANIE...
#10306128 SPARK PLUG BLOWOUT ON 1999 FORD F150 WITH 5.4L TRITON V8. IT SEEMS TO BE A VERY COMMON PROBLEM WITH THE FORD MODULAR ...
#10278266 ACCELERATING ON RAMP TO FREEWAY HEARD A LOUD BANG, VEHICLE LOST POWER AND ENGINE RAN ROUGH WHILE MAKING LOUD UNMUFFLE...
#10263567 ON FOUR SEPARATE OCCASIONS, THE VEHICLE BEGAN IDLING AND ACCELERATING ROUGHLY FOR ABOUT 2 DAYS. THE CHECK ENGINE LIG...
#10261090 WENT OUTSIDE TO START MY TRUCK 1999 FORD F-150 5.4L. AS SOON AS I STARTED THE TRUCK I HEARD A LOUD BANGING, SHUT THE ...

Recent Complaints for the 1999 FORD F-150

#11534217 VEHICLE SPEED CONTROL The contact owned a 1999 Ford F-150. The contact stated that he had parked the vehicle and was standing outside of th...
#11404509 ENGINE TL* THE CONTACT OWNED A 1999 FORD F-150. THE CONTACT STATED WHILE THE VEHICLE WAS PARKED AT HIS RESIDENCE, THE VEHICL...
#11360722 ENGINE LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722 EXTERIOR LIGHTING LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722 POWER TRAIN LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
Check any vehicle history by VIN - Free vehicle history report