NHTSA Complaint #10171390 — 1999 FORD F-150
ENGINE AND ENGINE COOLING:ENGINE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10171390 |
| Vehicle | 1999 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING:ENGINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 81,791 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | OH |
Consumer Description
I PURCHASED MY '99 FORD F-150 IN THE SPRING OF '04. AT THE TIME OF PURCHASE THE TRUCK HAD JUST OVER 49,000 MILES ON IT. THIS PAST MONDAY (10/16/06) WHILE PULLING OUT OF A LOCAL PARKING LOT, THE #2 SPARK PLUG WAS EJECTED OUT OF THE RIGHT CYLINDER HEAD, RIPPING OUT THE THREADS THAT THE SPARK PLUG SCREWS INTO & DESTROYING THE COIL PACK LOCATED DIRECTLY ABOVE. MY TRUCK ON THE DAY OF FAILURE HAD 81,790 MILES ON IT. THAT'S 18,210 MILES SHORT IF THE TRUCKS FIRST MANUFACTURES SUGGESTED 100,000 MILE TUNE-UP. FORD WILL NOT EVEN CONSIDER THE THOUGHT OF MAKING THIS MANUFACTURER'S DEFECT RIGHT. THEY SIMPLY TOLD ME THAT THE HEAD WOULD NEED TO BE REPLACED AT MY EXPENSE AND AT THE COST OF $2,800.00 TO $3,000.00. IT'S A DESIGN FLAW!!! THE ALUMINUM HEADS FOR THE 5.4 L ENGINES WERE ENGINEERED WITH AN INADEQUATE NUMBER OF THREADS NEEDED TO RETAIN THE SPARK PLUGS. THERE ARE ONLY 4 TO 5 THREADS TAPPED INTO THESE HEADS (APPROX. 1/4" TO 5/16" IN LENGTH) TODAY IS OCTOBER 19TH AND I HAVE PURCHASED A REPAIR KIT MANUFACTURED BY DORMAN PRODUCTS TO FIX THIS STRIPPED OUT SPARK PLUG MYSELF. THIS KIT IS SPECIFICALLY MADE BY DORMAN NOT FORD, TO FIX THIS PROBLEM OF FORDS 5.4L ENGINES. IT'S REALLY SAD THAT FORD HAS TO USE THE CONSUMERS AS GUINEA PIGS AND THEN FAIL SO MISERABLY TO BACK THEIR PRODUCT. I'M HESITANT TO CHECK THE TORQUE OF THE OTHER SEVEN PLUGS IN FEAR THAT THEY WILL NOT WITHSTAND THE RECOMMENDED 25 FOOT POUNDS OF TORQUE REQUIRED TO TIGHTEN THEM UP BUT IF I DON'T THEN IT'S RUSSIA ROULETTE AS TO WHEN THE NEXT ONE WILL BLOW OUT AND WHERE I WILL BE STRANDED WHEN IT DOES. I EXPECT FORD TO STAND BEHIND THEIR PRODUCT 110%, ESPECIALLY WHEN IT IS A WELL KNOWN FACT BY FORD AND THE CONSUMER THAT THERE IS AN ENGINEERING FLAW WITH THE DESIGN OF THE 5.4L ENGINES ALUMINUM HEADS PRODUCED BETWEEN YEARS OF 1997 THROUGH 2002. *NM
Related Complaints for the 1999 FORD F-150
Other ENGINE AND ENGINE COOLING:ENGINE Complaints
#10392544
WHILE DRIVING 45MPH ON SUBURBAN TWO LANE HIGHWAY I HEARD A LOUD BANG AND SUBSEQUENT RHYTHMIC POPPING SOUND ACCOMPANIE...
#10306128
SPARK PLUG BLOWOUT ON 1999 FORD F150 WITH 5.4L TRITON V8. IT SEEMS TO BE A VERY COMMON PROBLEM WITH THE FORD MODULAR ...
#10278266
ACCELERATING ON RAMP TO FREEWAY HEARD A LOUD BANG, VEHICLE LOST POWER AND ENGINE RAN ROUGH WHILE MAKING LOUD UNMUFFLE...
#10263567
ON FOUR SEPARATE OCCASIONS, THE VEHICLE BEGAN IDLING AND ACCELERATING ROUGHLY FOR ABOUT 2 DAYS. THE CHECK ENGINE LIG...
#10261090
WENT OUTSIDE TO START MY TRUCK 1999 FORD F-150 5.4L. AS SOON AS I STARTED THE TRUCK I HEARD A LOUD BANGING, SHUT THE ...
Recent Complaints for the 1999 FORD F-150
#11534217
VEHICLE SPEED CONTROL
The contact owned a 1999 Ford F-150. The contact stated that he had parked the vehicle and was standing outside of th...
#11404509
ENGINE
TL* THE CONTACT OWNED A 1999 FORD F-150. THE CONTACT STATED WHILE THE VEHICLE WAS PARKED AT HIS RESIDENCE, THE VEHICL...
#11360722
ENGINE
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722
EXTERIOR LIGHTING
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...
#11360722
POWER TRAIN
LOWER INTAKE MANIFOLD GASKETS KEEP BLOWING, AS WELL AS THE HEAD GASKETS I ONLY DRIVE FORD'S, SO FORD PLEASE FIX THIS ...