NHTSA Complaint #10143321 — 1998 PONTIAC BONNEVILLE
ENGINE AND ENGINE COOLING:ENGINE:GASOLINE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10143321 |
| Vehicle | 1998 PONTIAC BONNEVILLE |
| Component | ENGINE AND ENGINE COOLING:ENGINE:GASOLINE |
| Date of Incident | |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | FL |
Consumer Description
IT IS VERY OBVIOUS THAT GMC IS REFUSING TO ACKNOWLEDGE THE APPARENT DEFECTS WITH THE PONTIAC BONNEVILLE. MY ENGINE LOCKED UP IN JULY 2001 WITH NO PRIOR WARNING. THE MECHANIC THAT REPAIRED THE CAR TOLD ME THAT WATER AND RADIATOR FLUID WAS COMING OUT OF THE ENGINE AND THE CHEAP PLASTIC PLENTUM HAD TO BE REPLACED. NOW,THE SAME EXACT PROBLEM HAS OCCURRED ONCE AGAIN ON 11/07/2005. THE CAR WAS ONLY GOING 35 MPH WHEN THE ENGINE OVER-HEATED AND THIS TIME IT IS COSTING ME 2,321.00! I FEEL SOMETHING SHOULD BE DONE BY GMC OR RESEARCH SHOULD BE DONE TO RESOLVE THIS PROBLEM. IT IS EXTREMELY APPARENT THAT THIS IS A DEFECT IN ALL 1998 PONTIAC BONNEVILLES AND SOMETHING SHOULD BE DONE TO ADDRESS THE PROBLEM. I HAVE 3 CHILDREN AND CANNOT AFFORD A NEW CAR NOR CAN I AFFORD TO RE-BUILD OR RE-PLACE MY ENGINE EVERY 3-4 YEARS. *JB
Related Complaints for the 1998 PONTIAC BONNEVILLE
Other ENGINE AND ENGINE COOLING:ENGINE:GASOLINE Complaints
#10170734
THE 3800 ENGINE IN MY PONTIAC HAS IN THE PAST TWO YEARS FOR SOME REASON HAS HAD TO HAVE THE INTAKE MANIFOLD REPLACED ...
#10120911
THE INTAKE MANIFOLD GASKET (PLENUM) FAILED COSTING ME $2000 IN REPAIRS. THE GASKET HAD BEEN MADE OF A FAULTY PLASTIC ...
#10116418
FOR THE SECOND TIME IN ABOUT 2 YEARS MY 98 BONNEVILLE HAD THE PLENUM CRACK WHILE SIMPLY DRIVING AT NORMAL SPEEDS. THI...
#10056533
THE FUEL PRESSURE REGULATOR LEAKED GASOLINE; ALLOWING FUEL TO ENTER THE INTAKE MANIFOLD THROUGH A VACUUM LINE. A SPA...
#10052471
ENGINE/COOLING SYSTEM. *AK
Recent Complaints for the 1998 PONTIAC BONNEVILLE
#10764467
ENGINE
ENGINE COMPARTMENT FIRE APPROXIMATELY 30 MINS AFTER SHUTDOWN. INCIDENT 2015-00001363
#10713247
ENGINE AND ENGINE COOLING
THE BACK TWO CRADLE MOUNTS ON BOTH SIDES RUSTED OUT AND MOUNTS PULLED THROUGH THE CRADLE CAUSING THE STEERING TO BECO...
#10713247
POWER TRAIN
THE BACK TWO CRADLE MOUNTS ON BOTH SIDES RUSTED OUT AND MOUNTS PULLED THROUGH THE CRADLE CAUSING THE STEERING TO BECO...
#10713247
SERVICE BRAKES
THE BACK TWO CRADLE MOUNTS ON BOTH SIDES RUSTED OUT AND MOUNTS PULLED THROUGH THE CRADLE CAUSING THE STEERING TO BECO...
#10713247
STEERING
THE BACK TWO CRADLE MOUNTS ON BOTH SIDES RUSTED OUT AND MOUNTS PULLED THROUGH THE CRADLE CAUSING THE STEERING TO BECO...