NHTSA Complaint #10138439 — 1998 FORD F-150
ENGINE AND ENGINE COOLING issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10138439 |
| Vehicle | 1998 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | 117,100 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | NJ |
Consumer Description
TO WHOM IT MAY CONCERN: I AM THE OWNER OF A 1998 FORD F-150 4.2L XLT. A FEW WEEKS AGO I NOTICED A SLIGHT HESITATION UPON STARTING MY ENGINE. ONCE THE ENGINE STARTED, IT STRUGGLED A LITTLE AND THEN SMOOTHED OUT ONCE I BEGAN TO DRIVE. THE TRUCK CONTINUED TO RUN FINE, ONCE STARTED, BUT CONTINUED WITH THE SLIGHT HESITATION WHEN STARTING THE ENGINE FOR ABOUT A WEEK. ON SEPTEMBER 1, 2005, I ATTEMPTED TO START MY TRUCK AND FOUND THAT IT WOULD NOT TURN OVER RIGHT AWAY. I LET THE TRUCK REST A MOMENT THEN AGAIN ATTEMPTED TO START THE ENGINE. THE TRUCK STARTED UP, THEN I HEARD THE SLIGHT HESITATION AND ALL OF SUDDEN I HEARD A LOUD BANG FOLLOWED BY A LOUD NOISE COMING FROM THE ENGINE. I HAD THE TRUCK TOWED TO MY MECHANIC WHEREUPON I WAS INFORMED THAT IT WAS A ROD KNOCK, WHICH SHOT DOWN THROUGH THE OIL PAN. HE FOUND COOLANT ON THE PLUGS AND WATER INTRUSION THROUGH THE INTAKE MANIFOLD INTO THE BLOCK. HE INFORMED ME THAT MY ENGINE HAD HYDRO-LOCKED. THROUGH RESEARCH I WAS ABLE TO DETERMINE THAT THIS IS AN APPARENTLY WIDESPREAD PROBLEM. I FOUND THAT FORD MOTOR COMPANY ISSUED A RECALL ON THE INTAKE MANIFOLD GASKET IN 1999. I NEVER RECEIVED SUCH NOTIFICATION, ALTHOUGH I HAVE, IN FACT RECEIVED INFORMATION FOR OTHER RECALLS. I WAS NEVER SENT ANYTHING IN THE MAIL AND HAD NO IDEA OF THIS PROBLEM. IN ADDITION, I AM INFORMED THAT FORD MOTOR COMPANY IS NOT DOING ANYTHING TO RECTIFY THIS MATTER WITH CUSTOMERS. I CURRENTLY HAVE 117,000 MILES ON MY TRUCK AND HAD TO PAY OVER $4,000.00 TO REPLACE THE LONG BLOCK. I HAD TO PAY TO REPAIR A PROBLEM THAT FORD OBVIOUSLY KNEW EXISTED. SINCE FORD WAS AWARE OF THE POTENTIAL DANGER OF DAMAGING THE ENGINE AND DID LITTLE, IF NOTHING, TO INFORM ITS CUSTOMERS OF THIS POTENTIAL DANGER, I FEEL THAT FORD MOTOR COMPANY SHOULD BE HELD, AT LEAST IN PART, LIABLE FOR THE DAMAGE INCURRED TO MY TRUCK AND TO MANY OF THOSE, LIKE MYSELF, WHO HAVE HAD THE SAME PROBLEM. I WOULD GREATLY APPRECIATE YOUR ASSISTANCE IN THIS MATTER. *JB
Related Complaints for the 1998 FORD F-150
Other ENGINE AND ENGINE COOLING Complaints
#10618224
TL* THE CONTACT OWNS A 1998 FORD F-150. THE CONTACT STATED THAT THE VEHICLE LEAKED ANTI FREEZE INTO THE NUMBER TWO C...
#10442366
HAD THE 7 CYLINDER SPARK PLUG SHOOT OUT OF THE HEAD AND STRIP THE THREADS. *TR
#10442371
TL* THE CONTACT OWNS A 1998 FORD F-150. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 25 MPH, A STRONG ODOR OF ...
#10438016
TL* THE CONTACT OWNS A 1998 FORD F150. THE CONTACT STATED THAT THE MANIFOLD BOLTS WERE ROTTED, CAUSING THE EXHAUST T...
#10436097
TL* THE CONTACT OWNS A 1998 FORD F-150. THE CONTACT STATED THAT THE ENGINE CAUGHT ON FIRE WHILE THE VEHICLE WAS PARKE...
Recent Complaints for the 1998 FORD F-150
#11560757
STRUCTURE:BODY
1998 Ford F150 S/N 1FTRX18L7WNB03063 Mechanic said the frame is rusting badly. Suggested I not pull a heavy traile...
#11560757
UNKNOWN OR OTHER
1998 Ford F150 S/N 1FTRX18L7WNB03063 Mechanic said the frame is rusting badly. Suggested I not pull a heavy traile...
#11503088
FUEL/PROPULSION SYSTEM
My driver's side seat belt does not work at all for the past 6-8 months its been stuck and locked and it doesn't rele...