NHTSA Complaint #10104166 — 2002 FORD F SUPER DUTY
ENGINE AND ENGINE COOLING issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10104166 |
| Vehicle | 2002 FORD F SUPER DUTY |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | 70,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | MA |
Consumer Description
2002 FORD F250 SUPERDUTY V10- ENGINE. DRIVING TO WORK AT ABOUT 15 MPH. HEARD A LOUD BANG FROM ENGINE COMPARTMENT, ENGINE STARTED TO IDLE ROUGH, EXHAUST SMELL AND LOUD POPPING NOISE FROM ENGINE, TOWED TO DEALER WAYSIDE FORD MARLBORUGH MA., VERIFIED SPARK PLUG BLOWN OUT OF HEAD. TRUCK HAS BEEN DEALER MAINTAINED. CURRENTLY HAS ABOUT $70K MILES. PLUGS ARE NOT SCHEDULED TO BE CHANGED UNTIL 100K MILES. TRUCK IS NOT DRIVALBE, ESTIMATE ABOUT $300.00 TO REPLCE HEAD AND COIL. WAITING FOR RESPONSE FROM FORD FOR HELP. THIS IS A COMMOM PROBLEM PER DEALER AND OWNERS GROUPS.*AK
Related Complaints for the 2002 FORD F SUPER DUTY
Other ENGINE AND ENGINE COOLING Complaints
#10456254
WENT TO START MY TRUCK AND THAT'S WHEN THE SPARK PLUG BLEW OUT. *TR
#10444842
INJECTOR DRIVE MODULE (IDM), DIESEL 7.3 NAVISTAR ENGINE. IDM FAILED WHERE THE LIKELY CAUSE WAS WATER INFILTRATION ...
#10429127
SPARK PLUG BLOWOUT. *TR
#10424758
THE #9 SPARK PLUG SHOT OUT 9000 MILES AFTER THE FORD DEALERSHIP REPLACED ALL 10 PLUGS FOR $270. I WAS TOLD BY ALL PRI...
#10317466
THROWN SPARK PLUG FROM 2002 F-250. *TR
Recent Complaints for the 2002 FORD F SUPER DUTY
#10904574
TIRES
SET OF 5 UNIROYAL LIBERATOR TIRES PURCHASED NEW, LT265-75-16 LOAD RANGE E, 2002 F-250 4X4 (OEM SIZE) *THESE TIRES...
#10731993
SERVICE BRAKES
MY 2002 F250 SUPERDUTY WITH 7.3L DIESEL WILL NOT TURN AT PARKING SPEEDS AND HIGHER SPEEDS IF APPLYING THE BRAKE. I H...
#10731993
STEERING
MY 2002 F250 SUPERDUTY WITH 7.3L DIESEL WILL NOT TURN AT PARKING SPEEDS AND HIGHER SPEEDS IF APPLYING THE BRAKE. I H...
#10689548
ENGINE
TRAVELING ON A BUSY HIGHWAY AT 65 MPH; THE SPARK PLUG ON MY 5.4L V8 TRITON BLEW OUT OF ITS SOCKET. (ANY MECHANIC WILL...