NHTSA Complaint #10102614 — 2004 DODGE RAM 3500
SUSPENSION:FRONT:CONTROL ARM:UPPER BALL JOINT issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10102614 |
| Vehicle | 2004 DODGE RAM 3500 |
| Component | SUSPENSION:FRONT:CONTROL ARM:UPPER BALL JOINT |
| Date of Incident | |
| Date Filed | |
| Mileage | 22,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | PA |
Consumer Description
LOAD CLUNKING NOISE FROM FRONT AXLE, AND NOTICABLE INSTABILLITY IN STEERING ON BUMPY ROADS THAT ONLY STARTED WHEN THE FRONT BALL JOINTS DEVELOPED WHAT I BELEIVE TO BE EXCESSIVE WEAR. I MEASURED .033 VERTICLE FREE PLAY OF THE STEERING KNUCKLE, BUT MINIMAL LATERAL PLAY. ACCORDING TO DAIMLERCHRYSLER, THE -QUOTE- "NEW WAY OF CHECKING PLAY" ONLY REGISTERS .010 FREEPLAY, AND THE BALL JOINT HAS TO HAVE .060 TO BE DECLARE DEFECTIVE. AS SUCH DAIMLERCHRYSLER DENIED MY REPAIR. IN MY OPINION BY THE TIME THE LATERAL PLAY MEASURES .060, THE VERTICLE PLAY WILL DANGEROUSLY CLOSE TO CATASTROPHIC FAILURE. THERE HAVE BEEN NUMEROUS COMPLAINTS ABOUT THESE BALL JOINTS ON 2003 AND LATER "3RD GENERATION" 2500/3500 4 WHEEL DRIVE DODGE RAM HD PICKUPS ON THE VARIOUS INTERNET NEWS GROUPS, SUCH AS TURBO DIESEL REGISTER.COM.*AK
Related Complaints for the 2004 DODGE RAM 3500
Other SUSPENSION:FRONT:CONTROL ARM:UPPER BALL JOINT Complaints
Recent Complaints for the 2004 DODGE RAM 3500
#11686102
SUSPENSION
upper control arm cracked which is a safety violation and should be a recall. TRW 52106776 Control arm is the cracke...
#11461850
ENGINE
WHILE TRAVELING ON INTERSTATE 90 IN WASHINGTON STATE, TRAVELING AT ABOUT 60 MPH I NOTICED A HAZE BEHIND THE TRUCK THR...
#11461850
POWER TRAIN
WHILE TRAVELING ON INTERSTATE 90 IN WASHINGTON STATE, TRAVELING AT ABOUT 60 MPH I NOTICED A HAZE BEHIND THE TRUCK THR...
#11329101
FUEL/PROPULSION SYSTEM
STEERING BECAME LOOSE AND HAD 1-2INCHES OF SLACK BEFORE GUIDING THE VEHICLE PROPERLY. REPLACED WITH NEW STEERING UN...
#11329101
POWER TRAIN
STEERING BECAME LOOSE AND HAD 1-2INCHES OF SLACK BEFORE GUIDING THE VEHICLE PROPERLY. REPLACED WITH NEW STEERING UN...