NHTSA Complaint #10091761 — 2002 SUZUKI XL-7
ENGINE AND ENGINE COOLING issue reported to NHTSA
Complaint Details
| ODI Number | 10091761 |
| Vehicle | 2002 SUZUKI XL-7 |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | N/A miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | NY |
Consumer Description
PROBLEMS WITH VEHICLE OVERHEATING.*MR THE VEHICLE ENGINE WOULD OVERHEAT OCCASIONALLY AND LEAK COOLANT. THE VEHICLE WAS TAKEN TO THE DEALER WHO REPLACED THE COOLANT, RADIANT, THERMOSTAT AND OTHER ENGINE COMPONENTS. TRANSMISSION FLUID LEAKED AND WHITE SMOKE COULD BE SEEN COMING FROM THE REAR OF THE VEHICLE. THE VEHICLE'S ACCELERATOR PEDAL VIBRATED AND NOISE WAS HEARD COMING FROM THE ENGINE WHEN STARTING. THE TIMING CHAIN AND TENSIONER HAD TO BE REPLACED. *NM
Related Complaints for the 2002 SUZUKI XL-7
Other ENGINE AND ENGINE COOLING Complaints
#10479723
AC COMPRESSOR WENT OUT TWICE IN MY 2002 SUZUKI XL-7. ONCE IN AUGUST 2009 AND AGAIN IN MAY 2012. I HAD TO HAVE IT REPL...
#10361496
2002 SUZUKI XL7 A/C COMPRESSOR. WHILE DRIVING AT 65-70 MPH ON THE HIGHWAY, THE AIR CONDITIONING COMPRESSOR LOCKED UP ...
#10249614
I HAVE A 2002 SUZUKI XL-7 AND IN JAN 2005 NEWBURGH SUZUKI HAD TO REPLACE THE A/C COMPRESSOR BECAUSE LOCKED UP. VEH ON...
Recent Complaints for the 2002 SUZUKI XL-7
#10648401
STEERING
THIS 2002 SUZUKI XL7 LIMITED STARTED TO HAVE TOUCHY STEERING AT 55 MPH AND UP. IT IS SO SENSITIVE THAT IT CAN EVEN CH...
#10479723
STEERING
AC COMPRESSOR WENT OUT TWICE IN MY 2002 SUZUKI XL-7. ONCE IN AUGUST 2009 AND AGAIN IN MAY 2012. I HAD TO HAVE IT REPL...
#10479723
STRUCTURE:BODY
AC COMPRESSOR WENT OUT TWICE IN MY 2002 SUZUKI XL-7. ONCE IN AUGUST 2009 AND AGAIN IN MAY 2012. I HAD TO HAVE IT REPL...
#10459408
SUSPENSION
TL* THE CONTACT OWNS A 2002 SUZUKI XL7. THE CONTACT STATED THAT THE VEHICLE WOULD PULL TO THE RIGHT ABNORMALLY WHEN D...
#10429656
VEHICLE SPEED CONTROL
TL* THE CONTACT OWNS A 2002 SUZUKI XL7. WHILE DRIVING APPROXIMATELY 55 MPH, THE ACCELERATOR PEDAL WAS DEPRESSED AND T...