NHTSA Complaint #10057223 — 2000 LINCOLN LS
ELECTRICAL SYSTEM issue reported to NHTSA
Complaint Details
| ODI Number | 10057223 |
| Vehicle | 2000 LINCOLN LS |
| Component | ELECTRICAL SYSTEM |
| Date Filed | |
| Mileage | 27,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | NY |
Consumer Description
CONSUMER COMPLAINED ABOUT A REAR WINDOW PROBLEM. THE REAR WINDOW ON DRIVER'S SIDE WENT DOWN AND WOULD NOT GO BACK UP. THIS PROBLEM WAS CAUSED BY AN ELECTRICAL WIRING PROBLEM. *AK THE DEALER DETERMINED THAT THE WINDOW REGULATOR WAS JAMMED. THE DEALER REPLACED THE LEFT AND RIGHT REAR WINDOW REGULATOR. *NM
Related Complaints for the 2000 LINCOLN LS
Other ELECTRICAL SYSTEM Complaints
#10939508
TL* THE CONTACT OWNS A 2000 LINCOLN LS. WHILE DRIVING APPROXIMATELY 50 MPH, THE VEHICLE STALLED WITHOUT WARNING AND T...
#10467343
THE ENGINE FAILURES BEGAN ON JULY 28, 2005 AND HAVE CONTINUED THROUGH THIS DATE. THIS ENGINE SHOULD HAVE BEEN RECALL...
#10294400
2000 LINCOLN LS-COILS GO OUT AND THE CAR STALLS WHILE DRIVING ON INTERSTATE AND AT RED LIGHTS. *TR
#10257516
I BELIEVE MY 2000 LINCOLN LS IS UNSAFE TO DRIVE DO TO THE FACT THAT THE SHIFTING IS ERRATIC. THIS CAR HAS ACTUALLY CU...
#10256538
CHECK ADVANCTRAK LIGHT, BRAKE LIGHT AND TRACTION CONTROL LIGHT DISPLAY ILLUMINATE AND MILEAGE DISPLAYS LINES. *TR
Recent Complaints for the 2000 LINCOLN LS
#11246722
STEERING
BALL JOINT BOLTS LOOSEN OR DON'T TIGHTEN TO SPECIFICATIONS WHICH CAUSES A LOT OF WEAR AND TEAR ON THE FRONT END OF MY...
#11246722
SUSPENSION
BALL JOINT BOLTS LOOSEN OR DON'T TIGHTEN TO SPECIFICATIONS WHICH CAUSES A LOT OF WEAR AND TEAR ON THE FRONT END OF MY...
#11246722
UNKNOWN OR OTHER
BALL JOINT BOLTS LOOSEN OR DON'T TIGHTEN TO SPECIFICATIONS WHICH CAUSES A LOT OF WEAR AND TEAR ON THE FRONT END OF MY...
#11204822
AIR BAGS
TL* THE CONTACT OWNED A 2000 LINCOLN LS. WHILE DRIVING 35 MPH, THE STEERING WHEEL PULLED TO THE RIGHT AND CAUSED THE ...
#11204822
STEERING
TL* THE CONTACT OWNED A 2000 LINCOLN LS. WHILE DRIVING 35 MPH, THE STEERING WHEEL PULLED TO THE RIGHT AND CAUSED THE ...