NHTSA Complaint #10052535 — 1999 FORD F SUPER DUTY
ENGINE AND ENGINE COOLING:ENGINE:GASOLINE issue reported to NHTSA
Vehicle Towed
Complaint Details
| ODI Number | 10052535 |
| Vehicle | 1999 FORD F SUPER DUTY |
| Component | ENGINE AND ENGINE COOLING:ENGINE:GASOLINE |
| Date of Incident | |
| Date Filed | |
| Mileage | 51,707 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | Yes |
| State | AZ |
Consumer Description
AT LOW SPEED, SPARK PLUG BLEW OUT OF ENGINE, CAUSING LOUD EXHAUST NOISE AND GASOLINE FUMES WERE IMMEDIATELY SMELLED INSIDE PASSENGER COMPARTMENT. IF THIS WERE TO HAPPEN AT HIGH SPEED WITH ENGINE UNDER LOAD WHEN IMMEDIATE ENGINE SHUTDOWN WAS NOT SAFE OR POSSIBLE, THIS CONDITION WOULD CAUSE LARGE AMOUNTS GASOLINE/AIR MIXTURE TO BE EXPOSED TO HOT EXHAUST COMPONENTS, CAUSING FIRE HAZARD. IF THIS OCCURRED WHEN POWER WAS CRITICAL (PASSING OR TURNING IN FRONT OF TRAFFIC), THE LOSS OF POWER COULD ALSO CAUSE AN ACCIDENT. IF THIS OCCURRED WHEN DRIVING ON SLICK ROAD CONDITIONS, IT COULD CONTRIBUTE TO LOSS OF CONTROL OF VEHICLE. THIS IS CONSIDERED A "HEAVY DUTY" ENGINE, BUT DOES NOT USE A HARDENED THREADED INSERT IN THE CYLINDER HEADS TO STRENGTHEN THE THREADS THAT THE SPARK PLUGS SCREW INTO. SEARCHING ON THE INTERNET FOR (TRITON BLEW SPARKPLUG) REVEALS THAT THIS IS NOT AN ISOLATED INCIDENT. ALSO, THE MANUFACTURERS TORQUE SPECIFICATION FOR THE SPARK PLUGS IS QUITE LOW - PROBABLY DUE TO THE ALUMINUM THREADS IN THE HEAD. THIS COULD BE A CAUSE FOR THE SPARK PLUGS LOOSENING. *AK
Related Complaints for the 1999 FORD F SUPER DUTY
Other ENGINE AND ENGINE COOLING:ENGINE:GASOLINE Complaints
#8005509
ONGOING PROBLEM WITH THE VEHICLE HESITATING DURING ACCELERATION AND INTERMITTENTLY STALLING. VEHICLE BEEN TO DEALE...
#745262
ENGINE COMPLETELY LOST POWER, DUE TO RAIN WATER INGESTED INTO AIR BREATHER. *AK
#745263
NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK (TIRESIZE: 24570R19.5)( DOT NUMBER: TIRE SIZE: 24570R19.5 )
#740569
NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK
#726211
WHILE DRIVING AT 55/60 MPH THE ENGINE QUIT. WITH TOTAL LOSS OF POWER STEERING AND POWER BRAKES. THIS FAILURE NE...
Recent Complaints for the 1999 FORD F SUPER DUTY
#10579540
STEERING
1999.5 FORD-F350 DIESEL STEERING SECTOR SHAFT SNAPPED. DRIVING DOWN HIGHWAY, STEERING WHEEL WAS OFF 1/4 TURN. IN PA...
#10534170
FUEL SYSTEM, DIESEL
FUEL TANK STRAPS RUSTING FRONT AND REAR.....THE REAR STRAP BROKE ALLOWING FUEL TANK TO DROP. *TR
#10463944
FUEL/PROPULSION SYSTEM
VEHICLE HAD A FULL FUEL TANK (APPROX 38 GALLONS). VEHICLE WAS PARKED IN A SHOPPING PLAZA. WHEN I RETURNED TO THE VE...
#10460398
ENGINE
I BOUGHT THE TRUCK NEW IN 1999, AND NEVER HAD A PROBLEM UNTIL 2005 WHEN THE FIRST SPARK PLUG BLOW. IT COST ME $520.00...
#10425537
ELECTRICAL SYSTEM
FORD F-250 SUPER DUTY PICK UP TRUCK CAUGHT FIRE WHILE SITTING IN THE GARAGE. INSURANCE VEHICLE ARSON INVESTIGATOR DE...